Skip to Main Content

Incident Search

 
BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-25030SATER
12-19U
PDC ENERGY INC
69175
PA
6/13/2023
WATTENBERG
90750
WELD  123
SWNW 19 4N63W 6
306625
   
Search for Different Bradenhead:
County Code: Sequence Code:
 
Surface Casing Depth: 517 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403361253Form 173/28/20233/30/2023SHUT-IN48CONTINUOUS GASTSTM WHISPER 00Yes----Pre-P&A. 48 PSI continuous gas blew down to TSTM PSI within thirty minutes. PDC will schedule a sampling event and submit results via form 43.
Click for SpecificsFull1/27/20222/21/2022 34Continuous--0Down to Zero320320NoNoNo 
Click for SpecificsFull9/11/202112/21/2021 20Down to ZeroNone2Whisper (very low flow)340340NoNoneNone 
402418210Form 173/9/20206/10/2020 21DOWN TO 0 --0 NO FLOW 310310No----6 month follow-up test post abatement system install. PDC will continue to monitor pressure and report any increase in pressure to COGCC.
402239826Form 1711/10/201911/14/2019FLOWING160DOWN TO 0 --0 NO FLOW 410410No----Annual TEst 160 PSI blew down to 0 PSI within forst 60 seconds of test. No pressure or flow observed for the remainder of the test. PDC Will attempt to collect a sample and submit results to COGCC via form 43. PDC will submit a remediation plan via sundry.