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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-24219HOPPER
24-15
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
7/23/2019
WATTENBERG
90750
WELD  123
NESE 15 2N68W 6
336327
   
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Surface Casing Depth: 640 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
402072102Form 175/31/20196/12/2019PLUNGER LIFT1GAS --0 DOWN TO 0 12221221No----Surface casing produced no fluiid. Well shut in for 15min ended with no psi. Tubing shut in.
402030512Form 174/4/20195/2/2019PLUNGER LIFT1GAS --0 DOWN TO 0 14761476No----Surface casing produced no fluid. Well shut in for 15min ended with no psi. Tubing shut in.
400836273Form 174/21/20155/6/2015PLUNGER LIFT1GAS --0 DOWN TO 0 12831283No----POST REMEDIATION TEST. SURFACE CASING DID NOT PRODUCE ANY FLUID. 15 MINUTE BUILD-UP, DEAD. MASTER VALVE AND GROUND VALVE CLOSED UPON ARRIVAL. INITIAL POST REMEDIATION BLOW-DOWN ON 4-16-2015, STARTED WITH A WHISPER AND BLEW-DOWN TO 0 PSI.
400728540Form 1710/3/201411/11/2014PLUNGER LIFT22CONTINUOUS --0 DOWN TO 0 465474No----SC PRODUCED 10 GALLONS OF CONDENSATE. SHUT-IN WELL FOR 15 MINS, PRESSURED UP TO A WHISPER.
400404094Form 173/28/20134/15/2013PLUNGER LIFT11CONTINUOUS --0 DOWN TO 0 610611No----Surface casing produced 10 gallons of condensate during the form 17 test.
400286723Form 173/6/20125/18/2012PLUNGER LIFT26WATER H20 --<1 GAS 539542No----A small amount of water was produced during the first half of the test but turned into gas.