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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-23013PROMINENCE
4-8
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
1/6/2023
WATTENBERG
90750
WELD  123
NWNW 8 2N67W 6
305465
   
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Surface Casing Depth: 856 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403161896Form 178/31/20229/12/2022 3CONTINUOUS GAS0 NO FLOW 509511No----Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull7/19/20228/9/2022Plunger Lift3ContinuousNone--Whisper516518NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull7/26/20218/23/2021Plunger Lift2ContinuousNone--Whisper515516NoNN Tubing Shut in. Surface Casing produced no liquid.
402531086Form 1710/30/202011/12/2020 2WHISPER GAS0 NO FLOW 569568No----Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull12/6/201912/20/2019 6Gas--1Gas678678NoNoNoTubing shut in. Surface casing produced no liquids.
401766300Form 179/13/20189/18/2018 41GAS --1 WHISPER ----YesYes--Surface casing produced no fluids. Blew down surface casing an extra 30 min ended with a whisper. Surface casing shut in for 15 min ended with a whisper. Both tubing and casing were LOTO.
400647438Form 177/7/20147/21/2014PLUNGER LIFT474GAS --424 GAS 157178No----SURFACE CASING PRODUCED NO FLUID DURING FORM 17 TEST. MONITORED FOR AN ADDITIONAL 4 HOURS SHUT-IN SC WITH 4PSI CHECKED PRESSURE AFTER 15 MINUTES OF SHUT-IN TIME SC BULIT UP TO 29 PSI
400292340Form 174/18/20126/5/2012PLUNGER LIFT481GAS --314 GAS 466482No----No fluid was produced during 30 minute blow down