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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-19635POWERS RED X
27-16Di
KERR MCGEE OIL & GAS ONSHORE LP
47120
SI
8/1/2020
WATTENBERG
90750
WELD  123
SESE 27 2N65W 6
330791
   
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Surface Casing Depth: 1018 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull3/17/20257/21/2025 0No FlowNone0No Flow564564NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull11/12/202412/10/2024 2ContinuousNone--No Flow564565NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull7/28/20238/7/2023Plunger Lift2ContinuousNone--No Flow550550NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull5/24/20226/13/2022Plunger Lift1WhisperNone--No Flow536537NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull5/25/20216/14/2021Plunger Lift0No FlowNone--No Flow522522NoNoNo Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull10/9/202012/21/2020Plunger Lift1WHISPER ----DOWN TO 0 516517NoNoNo Tubing Shut in. Surface Casing produced no liquid.
402095416Form 177/1/20197/3/2019PLUNGER LIFT1WHISPER --0 DOWN TO 0 495495No----SURFACE CASING PRODUCED NO FLUIDS. 15 MINUTE SHUT IN RESULTED IN 0 PSI. TUBING LOTO.
400741954Form 1710/28/201411/26/2014PLUNGER LIFT1GAS --0 DOWN TO 0 429427No----SURFACE CASING PRODUCED NO FLUIDS DURING TEST. SHUT THE SURFACE CASING IN FOR 15 MINUTES PRESSURE STAYED AT 0 PSI. WELL SHUT IN UPON ARRIVAL.