Skip to Main Content

Incident Search

 
BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-11203HELMER GETZ UNIT TRUE
1
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
2/14/2022
WATTENBERG
90750
WELD  123
SWNW 18 1N66W 6
319407
   
Search for Different Bradenhead:
County Code: Sequence Code:
 
Surface Casing Depth: 979 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
402870458Form 1710/28/202111/15/2021 60CONTINUOUS GAS1 WHISPER 709707YesYesNoTubing Shut in. Surface Casing produced no liquid.
402592328Form 172/2/20212/5/2021 147CONTINUOUS GAS1 WHISPER 762761No----Tubing Shut in. Surface Casing produced no liquid.
402543954Form 1711/30/202012/1/2020 98CONTINUOUS GAS1 WHISPER 794784YesYesNoTubing Shut in. Surface Casing produced no liquid.
402099567Form 177/3/20197/9/2019PLUNGER LIFT210GAS --1 WHISPER 669669No---- Surface casing produced no fluids. 15 minute shut in resulted in whisper. 30 minute blow down resulted in whisper. Tubing shut in.
401060774Form 174/20/20166/9/2016 47GAS --1 GAS 128128No----SC DID NOT PRODUCE ANY FLUID. 30 MIN BLOWDOWN, WHISPER. 15 MIN BUILD UP, 3. INITIAL REMEDIATION BLOWDOWN ON 4-13-16 STARTED WITH 73 PSI AND BLEW DOWN TO A WHISPER.
400769658Form 1712/17/20141/13/2015PLUNGER LIFT107WATER H20 --18 WATER H20 400400No----Surface casing produced 20 gallons of water during test. Stopped test and shut in surface casing for 15 minutes pressure built up to 103 psi.
400352125Form 179/12/201211/30/2012PLUNGER LIFT59WATER H20 --<1 WATER H20 333333No----Surface casing produced 30 gallons of water.