404281238 | Form 17 | 7/8/2025 | 7/16/2025 | SHUT-IN | 348 | CONTINUOUS | GAS | 0 | WHISPER | 403 | 403 | No | -- | -- | This Form 17 submittal is associated with post-workover operations and a COA attached to ECMC Doc# 404141219.The test was performed through a two-inch valve. |
404091414 | Form 17 | 2/12/2025 | 2/12/2025 | SHUT-IN | 392 | CONTINUOUS | GAS | 0 | WHISPER | 392 | 391 | No | -- | -- | TEP has initiated a diagnostic evaluation for a potential casing repair based on the equalized pressures during the test. The test was performed through a 2" valve. |
Click for Specifics | Full | 2/22/2024 | 3/19/2024 | Plunger Lift | 421 | N/A | -- | 0 | Whisper | 420 | 420 | No | No | No | 1/2" blowdown |
Click for Specifics | Full | 11/6/2023 | 12/11/2023 | Plunger Lift | 448 | N/A | -- | 0 | Whisper | 448 | 449 | No | No | No | 1/2" blowdown |
403138616 | Form 17 | 8/15/2022 | 8/17/2022 | PLUNGER LIFT | 316 | NO FLOW | -- | 316 | NO FLOW | 316 | 316 | No | -- | -- | Per approval and guidance from the COGCC Area Engineer, a modified bradenhead test is being submitted to the COGCC due to pending remedial work on this well and safety concerns with performing a full bradenhead test at this time. TEP will perform a bradenhead test on the well after the proposed remedial work is complete and will submit the results to the COGCC via a Form 17. |
Click for Specifics | Full | 8/25/2021 | 9/6/2021 | Plunger Lift | 340 | N/A | -- | 330 | Continuous | 340 | 330 | No | No | No | |