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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-103-10374ANT HILL UNIT WYWATT
25-43
KT RESOURCES LLC
10775
SI
3/1/2024
WHITE RIVER
92800
RIO BLANCO  103
SWSE 25 2N97W 6
316367
   
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Surface Casing Depth: 1145 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403822520Form 176/5/20246/12/2024SHUT-IN22DOWN TO 0 VAPOR0 NO FLOW 655655No---- 
403767795Form 174/23/20244/24/2024SHUT-IN0NO FLOW NONE0 NO FLOW 668668No---- 
403593359Form 1711/10/202311/13/2023SHUT-IN1DOWN TO 0 NONE0 NO FLOW 620620No---- 
403276596Form 1712/22/202212/31/2022SHUT-IN0NO FLOW NONE0 NO FLOW 580580No----This bradenhead test has indicated that there is no communication between the surface casing (8.625") and the 5.5" production casing. The lack of communication between casings and the fact that the production casing pressure did not change when the bradenhead was opened indicates that this well has pressure integrity in with the production casing. In my opinion this well protects the health, safety, welfare, the environment and wildlife resources in the environment. It is requested that this bradenhead test be accepted has an alternative MIT as it has shown wellbore integrity and KT Resources has been unable to contract a workover rig due to high demand of equipment in the current price environment. If approved, this well will be turned into line.