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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-103-10142WRD UNIT
28-31
KT RESOURCES LLC
10775
SI
2/1/2024
WHITE RIVER
92800
RIO BLANCO  103
NWSW 28 2N96W 6
311837
   
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Surface Casing Depth: 1100 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403797023Form 175/15/20245/20/2024SHUT-IN0NO FLOW NONE0 NO FLOW 14201420No---- 
403756135Form 174/16/20244/16/2024SHUT-IN0NO FLOW NONE0 NO FLOW 14001400No---- 
403756101Form 174/16/20244/16/2024SHUT-IN0NO FLOW NONE0 NO FLOW 14001400No---- 
403438308Form 176/15/20236/19/2023SHUT-IN0NO FLOW NONE0 NO FLOW 14801480No---- 
403276692Form 1712/26/20221/1/2023SHUT-IN0NO FLOW NONE0 NO FLOW 14501450No----This bradenhead test has indicated that there is no communication between the surface casing (8.625") and the 5.5" production casing. The lack of communication between casings and the fact that the production casing pressure did not change when the bradenhead was opened indicates that this well has pressure integrity in with the production casing. In my opinion this well protects the health, safety, welfare, the environment and wildlife resources in the environment. It is requested that this bradenhead test be accepted has an alternative MIT as it has shown wellbore integrity and KT Resources has been unable to contract a workover rig due to high demand of equipment in the current price environment. If approved, this well will be turned into line.