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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-103-10130WRD FEDERAL
30-21
KT RESOURCES LLC
10775
SI
11/1/2023
WHITE RIVER
92800
RIO BLANCO  103
SWNW 30 2N96W 6
316269
   
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Surface Casing Depth: 1142 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
404129255Form 173/13/20253/16/2025SHUT-IN0NO FLOW NONE0 NO FLOW 780780No---- 
403821287Form 175/28/20246/11/2024SHUT-IN0NO FLOW NONE0 NO FLOW 745745No---- 
403805808Form 175/28/20245/29/2024SHUT-IN0NO FLOW NONE0 NO FLOW 745745No---- 
403763916Form 174/22/20244/22/2024SHUT-IN0NO FLOW NONE0 NO FLOW 720720No---- 
403445760Form 176/22/20236/26/2023SHUT-IN55DOWN TO 0 GAS0 NO FLOW 685685No---- 
403276580Form 1712/22/202212/31/2022SHUT-IN0NO FLOW NONE0 NO FLOW 460460No----This bradenhead test has indicated that there is no communication between the surface casing (8.625") and the 5.5" production casing. The lack of communication between casings and the fact that the production casing pressure did not change when the bradenhead was opened indicates that this well has pressure integrity in with the production casing. In my opinion this well protects the health, safety, welfare, the environment and wildlife resources in the environment. It is requested that this bradenhead test be accepted has an alternative MIT as it has shown wellbore integrity and KT Resources has been unable to contract a workover rig due to high demand of equipment in the current price environment. If approved, this well will be turned into line.