403797901 | Form 17 | 5/16/2024 | 5/21/2024 | SHUT-IN | 0 | NO FLOW | NONE | 0 | NO FLOW | 3 | 3 | No | -- | -- | |
403759202 | Form 17 | 4/17/2024 | 4/18/2024 | SHUT-IN | 6 | DOWN TO 0 | VAPOR | 0 | NO FLOW | 3 | 3 | No | -- | -- | |
403703901 | Form 17 | 2/25/2024 | 2/29/2024 | FLOWING | 0 | NO FLOW | NONE | 0 | NO FLOW | 0 | 0 | No | -- | -- | |
403593217 | Form 17 | 11/10/2023 | 11/13/2023 | FLOWING | 0 | NO FLOW | NONE | 0 | NO FLOW | 0 | 0 | No | -- | -- | |
403276772 | Form 17 | 12/31/2022 | 1/1/2023 | INJECTION | 0 | NO FLOW | NONE | 0 | NO FLOW | 0 | 0 | No | -- | -- | This bradenhead test has indicated that there is no communication between the surface casing (9.625") and the 7.0" production casing. The lack of communication between casings and the fact that the production casing pressure did not change when the bradenhead was opened indicates that this well has pressure integrity in with the production casing. In my opinion this well protects the health, safety, welfare, the environment and wildlife resources in the environment. It is requested that this bradenhead test be accepted has an alternative MIT as it has shown wellbore integrity and KT Resources has been unable to contract a workover rig due to high demand of equipment in the current price environment. If approved, this well will be turned into line.
NOTE: The tubing pressure from the beginning to the end of the test was negative 6 psig (vacuum). The form would not allow negative numbers so I input zeroes in. |