Skip to Main Content

Incident Search

 
BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-103-09924WRD UNIT
20-31
KT RESOURCES LLC
10775
SI
5/1/2020
WHITE RIVER
92800
RIO BLANCO  103
NWSW 20 2N96W 6
316157
   
Search for Different Bradenhead:
County Code: Sequence Code:
 
Surface Casing Depth: 1091 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403899848Form 178/21/20248/25/2024 0NO FLOW NONE0 NO FLOW 400400No---- 
403696946Form 172/21/20242/23/2024SHUT-IN20DOWN TO 0 VAPOR0 NO FLOW 440440No---- 
403441412Form 176/20/20236/21/2023SHUT-IN90DOWN TO 0 GAS0 NO FLOW 435435No---- 
403396156Form 176/16/20236/19/2023SHUT-IN0NO FLOW NONE0 NO FLOW 435435No---- 
403396177Form 175/3/20235/8/2023PLUNGER LIFT0NO FLOW NONE0 NO FLOW 460460No---- 
403247581Form 1711/30/202212/2/2022SHUT-IN0NO FLOW NONE0 NO FLOW 460460No----This breadenhead test has indicated that there is no communication between the surface casing (8.625") and the 5.5" production casing. The lack of communication between casings and the fact that the production casing pressure did not change when the bradenhead was opened indicates that this well has pressure integrity in with the production casing. In my opinion this well protects the health, safety, welfare, the environment and wildlife resources in the environment. It is requested that this bradenhead test be accepted has an alternative MIT as it has shown wellbore integrity and KT Resources has been unable to contract a workover rig due to high demand of equipment in the current price environment. If approved this well will be turned onto production.