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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-103-09920WRD UNIT
29-33
KT RESOURCES LLC
10775
SI
3/1/2024
WHITE RIVER
92800
RIO BLANCO  103
NWSE 29 2N96W 6
336394
   
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View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403797899Form 175/16/20245/21/2024SHUT-IN8DOWN TO 0 VAPOR0 NO FLOW 530530No---- 
403759200Form 174/17/20244/18/2024SHUT-IN45DOWN TO 0 VAPOR0 NO FLOW 520520No---- 
403700458Form 172/24/20242/27/2024FLOWING0NO FLOW NONE0 NO FLOW 5555No---- 
403439847Form 176/19/20236/20/2023SHUT-IN85DOWN TO 0 GAS0 NO FLOW 558558No---- 
403276762Form 1712/31/20221/1/2023PUMPING0NO FLOW NONE0 NO FLOW 100100No----This bradenhead test has indicated that there is no communication between the surface casing (7.000") and the 4.5" production casing. The lack of communication between casings and the fact that the production casing pressure did not change when the bradenhead was opened indicates that this well has pressure integrity in with the production casing. In my opinion this well protects the health, safety, welfare, the environment and wildlife resources in the environment. It is requested that this bradenhead test be accepted has an alternative MIT as it has shown wellbore integrity and KT Resources has been unable to contract a workover rig due to high demand of equipment in the current price environment. If approved, this well will be turned into line.