| 404327257 | Form 17 | 8/20/2025 | 8/22/2025 | INJECTION | 320 | CONTINUOUS | GAS | 0 | WHISPER | 11 | 11 | Yes | Yes | -- | 7 DAY BUILD UP. SURFACE CASING TIED INTO FLOWLINE. GAS SAMPLE TAKEN. SAMPLE ID: 05-103-06124
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| Click for Specifics | Full | 8/11/2025 | 12/15/2025 | | 110 | Continuous | -- | 0 | Whisper | 11 | 11 | No | No | No | |
| Click for Specifics | Full | 8/12/2024 | 9/4/2024 | | 345 | Continuous | -- | 0 | Whisper | 3 | 3 | No | No | No | |
| Click for Specifics | Full | 8/14/2023 | 9/5/2023 | Injector | 370 | Continuous | -- | 0 | No Flow | 30 | 30 | No | No | No | |
| Click for Specifics | Full | 8/17/2022 | 9/6/2022 | Injection | 400 | Down to Zero | -- | 0 | No Flow | 0 | 0 | No | No | No | |
| 402788191 | Form 17 | 8/17/2021 | 8/23/2021 | INJECTION | 412 | CONTINUOUS | GAS | 0 | DOWN TO 0 | 79 | 79 | No | -- | -- | Well has approved pressure management plan in place per Document # 402584723. We will continue to follow the approved plan to monitor and run diagnostics for the 1 year period ending on 1/27/2022. |
| 402555979 | Form 17 | 12/15/2020 | 12/17/2020 | INJECTION | 408 | CONTINUOUS | GAS AND VAPOR | 0 | WHISPER | 10 | 10 | Yes | Yes | -- | |
| 402467866 | Form 17 | 7/30/2020 | 8/17/2020 | INJECTION | 200 | GAS | -- | 0 | DOWN TO 0 | 139 | 140 | No | -- | -- | COGCC FIELD INSPECTION REPORT 693802365 NOTED HIGH BRADENHEAD PRESSURE, AFTER INSPECTION IT WAS NOTED THERE WAS A BAD GAUGE; REPLACED GAUGE AND READINGS WERE NORMAL. DISCUSSED WITH CHUCK BROWNING COGCC INSPECTOR AND HE SUGGESTED TO SUBMIT FORM 17 AS DOCUMENTATION OF CORRECTED GAUGE READINGS. |