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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-045-19626GGU Federal
42B-29-691
TEP ROCKY MOUNTAIN LLC
96850
PR
3/10/2011
MAMM CREEK
52500
GARFIELD  045
NWSE 29 6S91W 6
417787
   
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County Code: Sequence Code:
 
Surface Casing Depth: 836 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull5/13/20256/9/2025 0N/A--0No Flow247248NoNoNo2" Blowdown
Click for SpecificsFull5/22/20246/10/2024 0N/A--0No Flow245246NoNoNoBH is 2" Blowdown.
Click for SpecificsFull6/21/20237/17/2023Plunger Lift0N/A--0No Flow254256NoNoNo2" valve
Click for SpecificsFull3/14/20224/18/2022Plunger Lift0N/A--0No Flow266261NoNoNo2 inch ball valve
Click for SpecificsFull6/30/20217/12/2021Shut-In0N/A--0No Flow266267NoNoNo 
Click for SpecificsLight6/19/20196/2/2020 0  0 ----NoNoNo 
Click for SpecificsLight5/9/20176/2/2020 0  0 ----NoNoNo 
Click for SpecificsLight6/15/20166/2/2020 0  0 ----NoNoNo 
2221317Form 171/12/20111/20/2011SHUT-IN0NO FLOW --0 NO FLOW 00No----TUBING AND PRODUCTION CASING PRESSURES NOT REPORTED BY THE OPERATOR FOR THIS TEST. ACTUAL PRESSURES UNKNOWN, BUT ZERO WAS ENTERED FOR THE PRODUCTION CASING PRESSURE TO PROCESS THIS FORM AND AVOID FORM 17 VALIDATION ERRORS. OPERATOR COMMENTS: BRADENHEAD PRESSURE AFTER THE 7 DAY SHUT-IN PERIOD WAS 0 PSI. NO GAS SAMPLING OR BLOWDOWN TEST WAS RECORDED BECAUSE THE WELL HAD NO BRADENHEAD PRESSURE. THERE WAS NO PRODUCTION GAS SAMPLE BECAUSE THE WELL IS NOT PRODUCING.
Click for SpecificsLight11/4/20106/2/2020 --  0 ----NoNoNo 
Click for SpecificsLight10/21/20106/2/2020 --  -- ----NoNoNo