Skip to Main Content

Incident Search

 
BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-045-19619GGU Swanson
33C-29-691
TEP ROCKY MOUNTAIN LLC
96850
PR
3/30/2011
MAMM CREEK
52500
GARFIELD  045
NWSE 29 6S91W 6
417787
   
Search for Different Bradenhead:
County Code: Sequence Code:
 
Surface Casing Depth: 790 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull5/13/20256/9/2025 74N/A--0No Flow310312NoNoNo2" Blowdown
Click for SpecificsFull5/22/20246/10/2024 74N/A--0Whisper258259NoNoNoBH is 2" Blowdown.
Click for SpecificsFull6/21/20237/17/2023Plunger Lift84N/A--0No Flow267270NoNoNo2" valve
Click for SpecificsFull3/14/20224/18/2022Plunger Lift67N/A--0No Flow281262NoNoNo2 inch ball valve
Click for SpecificsFull6/30/20217/12/2021Shut-In68N/A--0Down to Zero251255NoNoNo 
Click for SpecificsLight6/19/20196/2/2020 0  0 ----NoNoNo 
Click for SpecificsLight5/9/20176/2/2020 0  0 ----NoNoNo 
Click for SpecificsLight6/15/20166/2/2020 12  0 ----NoNoNo 
2221318Form 171/12/20111/20/2011SHUT-IN10DOWN TO 0 --0 DOWN TO 0 00No----TUBING AND PRODUCTION CASING PRESSURES NOT REPORTED BY THE OPERATOR FOR THIS TEST. ACTUAL PRESSURES UNKNOWN, BUT ZERO WAS ENTERED FOR THE PRODUCTION CASING PRESSURE TO PROCESS THIS FORM AND AVOID FORM 17 VALIDATION ERRORS. OPERATOR COMMENTS: BRADENHEAD PRESSURE AFTER 7 DAY SHUT-IN WAS 10 PSI. NO GAS SAMPLING OR BLOWDOWN TEST WAS RECORDED BECAUSE THE PRESSURE BLEW DOWN IMMEDIATELY. THE BRADENHEAD WAS LEFT OPEN TO VENT AFTER THE BRADENHEAD TEST WAS CONDUCTED. THERE WAS NO PRODUCTION GAS SAMPLE BECAUSE THE WELL IS NOT PRODUCING.
Click for SpecificsLight11/9/20106/2/2020 --  0 ----NoNoNo 
Click for SpecificsLight10/26/20106/2/2020 --  -- ----NoNoNo