| Click for Specifics | Full | 5/14/2025 | 6/9/2025 | | 11 | N/A | -- | 0 | No Flow | 205 | 193 | No | No | No | 1/2" BH, CYCLED DURING TEST |
| Click for Specifics | Full | 2/15/2024 | 3/19/2024 | Plunger Lift | 6 | N/A | -- | 0 | No Flow | 332 | 298 | No | No | No | 2" bh |
| Click for Specifics | Full | 7/25/2023 | 8/14/2023 | Plunger Lift | 24 | N/A | -- | 0 | No Flow | 249 | 261 | No | No | No | 1/2" BH |
| 403262985 | Form 17 | 12/15/2022 | 12/15/2022 | PLUNGER LIFT | 189 | NO FLOW | -- | 189 | NO FLOW | 200 | 200 | No | -- | -- | Per approval and guidance from the COGCC Area Engineer, a modified bradenhead test is being submitted to the COGCC due to a recently identified production casing issue and safety concerns with performing a full bradenhead test at this time. TEP will be submitting a Form 4 which will report the results of diagnostic testing and the proposed well repair procedure. |
| Click for Specifics | Full | 4/1/2022 | 5/16/2022 | Plunger Lift | 0 | N/A | -- | 0 | No Flow | 201 | 193 | No | No | No | Blow down 1/2” |
| Click for Specifics | Full | 5/13/2021 | 6/7/2021 | Plunger Lift | 0 | N/A | -- | 0 | No Flow | 200 | 208 | No | No | No | |
| Click for Specifics | Light | 10/1/2019 | 6/2/2020 | | 0 | | | 0 | | -- | -- | No | No | No | |
| Click for Specifics | Light | 10/1/2017 | 6/2/2020 | | 0 | | | 0 | | -- | -- | Yes | Yes | No | |
| Click for Specifics | Light | 1/1/2016 | 6/2/2020 | | 0 | | | 0 | | -- | -- | Yes | No | Yes | |
| Click for Specifics | Light | 10/1/2015 | 6/2/2020 | | -- | | | 0 | | -- | -- | No | No | No | |
| Click for Specifics | Light | 9/9/2014 | 6/2/2020 | | 0 | | | 0 | | -- | -- | No | No | No | 0 min. |
| Click for Specifics | Light | 9/11/2013 | 6/2/2020 | | 2 | | | 0 | | -- | -- | No | No | No | |
| Click for Specifics | Light | 10/29/2012 | 6/2/2020 | | 2 | | Gas | 0 | | -- | -- | Yes | Yes | No | |
| Click for Specifics | Light | 10/25/2011 | 6/2/2020 | | 10 | | Gas | 0 | | -- | -- | Yes | Yes | No | |