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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-001-10492GUS LD
34-373HC
PDC ENERGY INC
69175
PR
1/23/2021
WATTENBERG
90750
ADAMS  001
SENE 21 1S67W 6
476754
   
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Surface Casing Depth: 2045 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
404184191Form 174/14/20254/30/2025GAS LIFT10CONTINUOUS GAS1 WHISPER 547540No----Remediation follow up test. 10 PSI whisper gas, blew down to 1 within thirty minutes, whisper gas continued for entire test. Operator will monitor pressure and re-test according to bradenhead policy.
403774797Form 174/26/20244/30/2024 4DOWN TO 0 GAS0 NO FLOW 957993No----Abatement system follow up test - 4 PSI gas flow blew down to 0 PSI within first minute of test. No pressure or flow observed for the remainder of the test. PDC will monitor pressure and re-test according to bradenhead policy.
403381637Form 174/20/20234/24/2023PLUNGER LIFT0DOWN TO 0 GAS0 NO FLOW 20052005No----Post-Production test within 60 days of first sales. 0 PSI, no pressure or flow observed for the entire test. PDC will monitor bradenhead pressure monthly and submit annual test.
Click for SpecificsFull10/17/202211/8/2022Shut-In0Down to Zero--0Down to Zero14251425NoNoneNone 
402597202Form 172/1/20212/10/2021FLOWING1WHISPER GAS0 NO FLOW 22032180No----Test after DOFP. Whisper on open for 8 minutes and died. No flow for the remainder of the test.
402565515Form 1712/26/20201/4/2021SHUT-IN0NO FLOW NONE0 NO FLOW 00No----Test prior to toe-prep/frac. Vacuum on open for 20 seconds on open.
402523025Form 1710/22/202010/30/2020SHUT-IN-10NO FLOW --0 NO FLOW ----No----Test after rig release. Vaccum at open for 10 minutes then dead.