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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-001-10481Kortum LD
09-376HC
PDC ENERGY INC
69175
PR
2/20/2022
WATTENBERG
90750
ADAMS  001
NWNE 21 1S67W 6
443415
   
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Surface Casing Depth: 2065 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull11/7/202511/17/2025 10Continuous--0No Flow453453NoNoNo Annual Test.  10 PSI blew down to 0 PSI within first few seconds of test.  No pressure or flow observed for the remainder of the test. Operator will monitor pressure and re-test according to bradenhead policy.
404196777Form 174/22/20255/8/2025GAS LIFT5CONTINUOUS GAS1 WHISPER 659659No----Remediation follow up test. 5 PSI continuous gas flow blew down to 1 PSI within thirty minutes. Whisper gas continued for entire test. Operator will monitor pressure and re-test according to bradenhead policy.
Click for SpecificsFull4/26/20244/30/2024 8Down to Zero--0Down to Zero14821561NoNoNo 
403326824Form 172/17/20232/22/2023FLOWING335DOWN TO 0 MUD0 CONTINUOUS 17981810Yes----Post-Production within 30 days of first sales. 335 PSI mud on open, collected BH and production samples. Produced ~6 gallons of mud and died. Mud started again at the 10 minute mark and dripped/trickled for remainder of test. Produced ~6.5 gallons total.
403095542Form 177/1/20227/5/2022SHUT-IN0NO FLOW --0 NO FLOW 00No----Initial Test Post Rig Release. 0 PSI, no pressure or flow observed for the entire 30 min test. PDC will monitor pressure and re-test according to bradenhead policy.