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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-001-10477Kortum LD
09-378HNX
PDC ENERGY INC
69175
PR
3/10/2023
WATTENBERG
90750
ADAMS  001
NWNE 21 1S67W 6
443415
   
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Surface Casing Depth: 2060 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull11/7/202511/17/2025 12Continuous--0No Flow242292NoNoNo Annual Test.  12 PSI blew down to 0 PSI within first few seconds of test.  No pressure or flow observed for the remainder of the test. Operator will monitor pressure and re-test according to bradenhead policy.
404196783Form 174/22/20255/8/2025GAS LIFT3CONTINUOUS GAS1 WHISPER 527523No----Remediation follow up test. 3 PSI continuous gas flow blew down to 1 PSI within thirty minutes. Whisper gas continued for entire test. Operator will monitor pressure and re-test according to bradenhead policy.
Click for SpecificsFull4/26/20244/30/2024 5Down to Zero--0Down to Zero704704NoNoNo 
403329696Form 172/22/20232/24/2023FLOWING660DOWN TO 0 MUD0 CONTINUOUS 23892387Yes----Post-Production test within 30 days of first sales. 660 PSI, mud on open. Produced 12 gallons and died to trickle in less than 5 minutes. Trickle for duration of test, produced ~12.5 gallons total. PDC will monitor pressure and re-test according to bradenhead policy.
403095555Form 177/1/20227/5/2022SHUT-IN0NO FLOW --0 NO FLOW 00No----Initial Test Post Rig Release. 0 PSI, no pressure or flow observed for the entire 30 min test. PDC will monitor pressure and re-test according to bradenhead policy.