| Click for Specifics | Full | 11/7/2025 | 11/17/2025 | | 12 | Continuous | -- | 0 | No Flow | 242 | 292 | No | No | No | Annual Test. 12 PSI blew down to 0 PSI within first few seconds of test. No pressure or flow observed for the remainder of the test. Operator will monitor pressure and re-test according to bradenhead policy. |
| 404196783 | Form 17 | 4/22/2025 | 5/8/2025 | GAS LIFT | 3 | CONTINUOUS | GAS | 1 | WHISPER | 527 | 523 | No | -- | -- | Remediation follow up test. 3 PSI continuous gas flow blew down to 1 PSI within thirty minutes. Whisper gas continued for entire test. Operator will monitor pressure and re-test according to bradenhead policy. |
| Click for Specifics | Full | 4/26/2024 | 4/30/2024 | | 5 | Down to Zero | -- | 0 | Down to Zero | 704 | 704 | No | No | No | |
| 403329696 | Form 17 | 2/22/2023 | 2/24/2023 | FLOWING | 660 | DOWN TO 0 | MUD | 0 | CONTINUOUS | 2389 | 2387 | Yes | -- | -- | Post-Production test within 30 days of first sales. 660 PSI, mud on open. Produced 12 gallons and died to trickle in less than 5 minutes. Trickle for duration of test, produced ~12.5 gallons total. PDC will monitor pressure and re-test according to bradenhead policy. |
| 403095555 | Form 17 | 7/1/2022 | 7/5/2022 | SHUT-IN | 0 | NO FLOW | -- | 0 | NO FLOW | 0 | 0 | No | -- | -- | Initial Test Post Rig Release. 0 PSI, no pressure or flow observed for the entire 30 min test. PDC will monitor pressure and re-test according to bradenhead policy. |