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 Surface Location
 API# 05-121-11053
Well Classification: DSPW Status: IJ - 2/1/2018
Well Name/No:Buzzs Boat #14
(Click Well Name for Production Data)
Click Here for Transporter Gatherer Info
Operator:GRAND MESA OPERATING CO - 35080
(Click Operator Name for Company Detail Report)
Federal Or State Lease #:
Facility Status:IJStatus Date2/1/2018
FacilityID:442963LocationID:442964
County:WASHINGTON #121Location:SESW 24 5S54W 6
Field:WILDCAT - #99999Elevation:5152 ft.
Planned Location:620FSL  2262 FWLLat/Long: 39.595810 / -103.379510Lat/Long Source: Field Measured
As Drilled Location:Footages Not AvailableLat/Long: 39.595810 / -103.379510Lat/Long Source: Field Measured
 Wellbore And Formation Details -- select either a wellbore Or formation to expand.
 

Wellbore #00             Wellbore Classification: OW             Status: IJ - 8/1/2018             Measured TD: 8254 ft.

 Wellbore Data for Original WellboreWellbore Classification: OW        IJ - 8/1/2018
Wellbore Permit
Permit #: Expiration Date:4/26/2019
Prop Depth/Form:8254 ft.
Surface Mineral Owner Same:No
Mineral Owner:FEESurface Owner:FEE
Unit: Unit Number:
Formation And Spacing:Code: CDHL , Formation: CEDAR HILLS , Order: , Unit Acreage: , Drill Unit:
Formation And Spacing:Code: CRTC , Formation: CRETACEOUS , Order: , Unit Acreage: , Drill Unit:
Formation And Spacing:Code: MSSP , Formation: MISSISSIPPIAN , Order: , Unit Acreage: , Drill Unit:
Formation And Spacing:Code: PENN , Formation: PENNSYLVANIAN , Order: , Unit Acreage: , Drill Unit:
Formation And Spacing:Code: WFCMP , Formation: WOLFCAMP , Order: , Unit Acreage: , Drill Unit:
Casing:String Type: SURF, Hole Size: 12.25 in., Size: 8.625 in., Top: 0 ft., Depth: 330 ft., Weight: 24 , Citings Type: PLANNED
Cement:Sacks: 225, Top: 0 ft., Bottom: 330 ft.
Casing:String Type: 1ST, Hole Size: 7.875 in., Size: 5.5 in., Top: 0 ft., Depth: 8228 ft., Weight: 17 , Citings Type: PLANNED
Cement:Sacks: 276, Top: 5308 ft., Bottom: 8254 ft.
Casing:String Type: S.C. 1.1, Hole Size: , Size: , Top: , Depth: , Weight: , Citings Type: PLANNED
Cement:Sacks: , Top: 4400 ft., Bottom: 5100 ft.
Casing:String Type: STAGE TOOL, Hole Size: , Size: , Top: , Depth: 5191 ft., Weight: , Citings Type: PLANNED
Cement:Sacks: 250, Top: 4034 ft., Bottom: 5191 ft.

Wellbore Completed
Completion Date:11/10/2016
Spud Date:10/30/2016Spud Date Is:ACTUAL
Measured TD:8254 ft.Measured PB depth:8191 ft.
True Vertical TD:True Vertical PB depth:
Log Types:AI Shallow Focused Elect log; CPDCN Micro Log; Comp Sonic w/Integrated Transit Time; Cement Bond Log
Casing:String Type: SURF, Hole Size: 12.25 in., Size: 8.625 in., Top: 0 ft., Depth: 330 ft., Weight: 24 , Citings Type: ACTUAL
Cement:Sacks: 225, Top: 0 ft., Bottom: 330 ft., Determination Method: VISU
Casing:String Type: 1ST, Hole Size: 7.875 in., Size: 5.5 in., Top: 0 ft., Depth: 8228 ft., Weight: 17 , Citings Type: ACTUAL
Cement:Sacks: 276, Top: 5308 ft., Bottom: 8254 ft., Determination Method: CBL
Additional Cement:String Type: 1ST , Top: 4034 ft., Depth: 5191 ft., Bottom: 5191 ft., Sacks: 250, Method: STAGE TOOL
FormationInterval TopLog BottomCoredDSTs
PIERRE325 ft.
SHARON SPRINGS3550 ft.
NIOBRARA3675 ft.
FORT HAYS4111 ft.4196 ft.NN
CEDAR HILLS5770 ft.5855 ft.NN
STONE CORRAL5973 ft.5983 ft.NN
WOLFCAMP6095 ft.
LANSING-KANSAS CITY6915 ft.7249 ft.NN
MARMATON7300 ft.7428 ft.NN
MISSISSIPPIAN8038 ft.8114 ft.NN

Formation MRTN                     Formation Classification:  DSPW                     Status:  AB - 9/13/2017                 Interval Top: 7364 ft.    Interval Bottom: 7428 ft.

 Completed Information for Formation MARMATON
1st Production Date:N/AChoke Size: 
Formation Name:MARMATONCommingled:No
Production Method:
Open Hole Completion:No
Formation Treatment
Treatment Type:ACID JOB
Treatment Date:1/17/2017Treatment End Date:1/31/2017
Treatment Summary:1/17/17 Perfed from 7416-7428' w/4shots per foot then pumped 250gals of 7.5 acid and pressured up to 1000#. 1/19/17 Perfed from 7394-7408 w/4shots per foot then pumped 250gals 15% MCA acid staged with 1000#. 1/23/17 Perfed from 7364-7370 w/4shots per foot then pumped 250gals 15% MCA acid into perfs at 1.5bbls min @ 500#. 1/24/17 Pumped 750gals 15% NE/FE acid into perfs at 2.5bbls min @ 650#. 1/25/17 Pumped 750gals 15% MCA acid into perfs staged on perfs @ 1500#. 1/31/17 Pumped 2000gals of 20% NE/FE acid and pressured up to 1400#, after displacing .5bbls acid was shown to be channeled up to perfs above the packer, moved the packer above the top perfs and set.
Total fluid used in treatment (bbls):241Max pressure during treatment (psi):1500
Total gas used in treatment (mcf):Fluid density (lbs/gal):
Type Of gas:Number Of staged intervals:
Total acid used in treatment (bbls):101Min frac gradient (psi/ft):
Recycled water used in treatment (bbls):140Total flowback volume recovered (bbls):0
Fresh water used in treatment (bbls):0Disposition method For flowback:RECYCLE
Total proppant used (lbs):Green completions techniques utilized:Yes
Reason green techniques Not utilized: 
Tubing Size:Tubing Setting Depth:
Tubing Packer Depth:Tubing Multiple Packer:
Open Hole Top:Open Hole Bottom:
Initial Test Data:
Test Date:N/ATest Method:
Hours Tested:Gas Type:
Gas Disposal:
Test TypeMeasure
BBLS_H2O 40
CALC_BBLS_H2O 40
Perforation Data:
Interval Top:7364 ft.# Of Holes:140
Interval Bottom:7428 ft.Hole Size:0.375 in.

Formation LGKC                     Formation Classification:  DSPW                     Status:  AB - 8/16/2017                 Interval Top: 6916 ft.    Interval Bottom: 7185 ft.

 Completed Information for Formation LANSING-KANSAS CITY
1st Production Date:N/AChoke Size: 
Formation Name:LANSING-KANSAS CITYCommingled:No
Production Method:
Open Hole Completion:No
Formation Treatment
Treatment Type:ACID JOB
Treatment Date:2/1/2017Treatment End Date:2/3/2017
Treatment Summary:2/1/17 perfed from 7176-7185' w 4/shots per foot, pumped 250gals of 15% MCA acid @ .6bbls min @ 1150# 2/2/17 pumped 750gals 15% MCA acid and displaced into perfs @ 2bbls/min @ 1550 2/3/17 Perfed from 6916-6922' w 4/shots per foot
Total fluid used in treatment (bbls):188Max pressure during treatment (psi):1550
Total gas used in treatment (mcf):Fluid density (lbs/gal):
Type Of gas:Number Of staged intervals:
Total acid used in treatment (bbls):24Min frac gradient (psi/ft):
Recycled water used in treatment (bbls):44Total flowback volume recovered (bbls):0
Fresh water used in treatment (bbls):120Disposition method For flowback:RECYCLE
Total proppant used (lbs):Green completions techniques utilized:Yes
Reason green techniques Not utilized: 
Tubing Size:Tubing Setting Depth:
Tubing Packer Depth:Tubing Multiple Packer:
Open Hole Top:Open Hole Bottom:
No Initial Test Data was found for formation LGKC.
Perforation Data:
Interval Top:6916 ft.# Of Holes:164
Interval Bottom:7185 ft.Hole Size:0.375 in.

Formation WFCMP                   Formation Classification:  DSPW                   Status:  IJ - 12/23/2020                Interval Top: 6290 ft.    Interval Bottom: 6320 ft.

 Completed Information for Formation WOLFCAMP
1st Production Date:2/13/2018Choke Size: 
Formation Name:WOLFCAMPCommingled:No
Production Method:
Open Hole Completion:No
Formation Treatment
Treatment Type:ACID JOB
Treatment Date:12/1/2020Treatment End Date:12/1/2020
Treatment Summary:12/1/2020 Pumped 20% DWA w/additives to clean perforations for SWD well.
Total fluid used in treatment (bbls):30Max pressure during treatment (psi):540
Total gas used in treatment (mcf):Fluid density (lbs/gal):
Type Of gas:Number Of staged intervals:
Total acid used in treatment (bbls):24Min frac gradient (psi/ft):
Recycled water used in treatment (bbls):Total flowback volume recovered (bbls):0
Fresh water used in treatment (bbls):6Disposition method For flowback:
Total proppant used (lbs):Green completions techniques utilized:--
Reason green techniques Not utilized: 
Formation Treatment
Treatment Type:
Treatment Date:3/5/2018Treatment End Date:N/A
Treatment Summary:Operator began injection on 2/13/2018.
Total fluid used in treatment (bbls):Max pressure during treatment (psi):
Total gas used in treatment (mcf):Fluid density (lbs/gal):
Type Of gas:Number Of staged intervals:
Total acid used in treatment (bbls):Min frac gradient (psi/ft):
Recycled water used in treatment (bbls):Total flowback volume recovered (bbls):
Fresh water used in treatment (bbls):Disposition method For flowback:
Total proppant used (lbs):Green completions techniques utilized:--
Reason green techniques Not utilized: 
Formation Treatment
Treatment Type:ACID JOB
Treatment Date:8/17/2017Treatment End Date:8/17/2017
Treatment Summary:500gals 15% NE/FE acid with 93bbls 2% KCL Biocide.
Total fluid used in treatment (bbls):105Max pressure during treatment (psi):1700
Total gas used in treatment (mcf):Fluid density (lbs/gal):
Type Of gas:Number Of staged intervals:
Total acid used in treatment (bbls):12Min frac gradient (psi/ft):
Recycled water used in treatment (bbls):93Total flowback volume recovered (bbls):105
Fresh water used in treatment (bbls):0Disposition method For flowback:RECYCLE
Total proppant used (lbs):0Green completions techniques utilized:Yes
Reason green techniques Not utilized: 
Tubing Size:2.875 in.Tubing Setting Depth:6264 ft.
Tubing Packer Depth:6258 ft.Tubing Multiple Packer:
Open Hole Top:Open Hole Bottom:
No Initial Test Data was found for formation WFCMP.
Perforation Data:
Interval Top:6290 ft.# Of Holes:124
Interval Bottom:6320 ft.Hole Size:0.375 in.
Primary Well Designation:
None      i
            All DesignationsDate
Reported PluggedN 
Out Of Service RepurposedN 
Out Of ServiceN 
Inactive ExceptionN 
Noticed InactiveN 
Defined InactiveN 
Low ProducingN 

BOE/MCFE/GOR Calculations
Production for Previous 12 Months
August 2023 - July 2024i
Total Oil Produced (Barrels)0
Total Gas Produced (MCF)0
GOR
GOR Determination 
Average BOE per Day0.000
Average MCFE per Day0.000

 Federal Financial Assurance  i 

 Tribal Well  i No