Formation Treatment |
Treatment Type: | |
Treatment Date: | 2/3/2022 | Treatment End Date: | N/A |
Treatment Summary: | High casing pressure was found on M.C. Hagood A19X the well was shut in, the workover consisted of pulling the injection tubing, and both the top & bottom packers, perform clean out, running new injection string and packers, and adding a TM-40 spool & hanger. Well to be returned to injection pending an approved Form 21. |
Total fluid used in treatment (bbls): | | Max pressure during treatment (psi): | |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 7/16/2021 | Treatment End Date: | 7/16/2021 |
Treatment Summary: | PUMPED 4000 GALLONS (95.2 BBLS) 15% HCL AND 6% CITRIC ACID WITH 45 BBLS WATER |
Total fluid used in treatment (bbls): | 140 | Max pressure during treatment (psi): | 2136 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 95 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 45 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 7/20/2017 | Treatment End Date: | 7/20/2017 |
Treatment Summary: | PUMPED 2000 GALLONS 15% HCL WIHT 110 GALLONS SOLVENT, 130 BBLS FRESH WATER |
Total fluid used in treatment (bbls): | 180 | Max pressure during treatment (psi): | |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 130 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Date: | 9/10/2009 |
Treatment Summary: | ACID STIMULATION 9/10/2009 PUMPED 4116 GALLONS OF 20% HCI ALTHROUGH TUBING AT 6401'. MAX TREATING PRESSURE OF 3.3 BPM @ 1747 PSI. |