Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 12/14/2022 | Treatment End Date: | 12/14/2022 |
Treatment Summary: | PUMPED 2000 GALLONS (47.6 BBLS) 15% HCL W/MUTUAL SOLVENT AND 35 BBLS WATER |
Total fluid used in treatment (bbls): | 82 | Max pressure during treatment (psi): | 2450 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 35 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 7/13/2019 | Treatment End Date: | 7/13/2019 |
Treatment Summary: | PUMPED 2000 GALLONS (47.6 BBLS) 15% HCL W/3% CITRIC ACID AND 45 BBLS WATER. |
Total fluid used in treatment (bbls): | 92 | Max pressure during treatment (psi): | 2156 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 45 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 8/6/2017 | Treatment End Date: | 8/7/2017 |
Treatment Summary: | PUMPED 4000 GALLONS 15% HCL WITH 160 BBLS WATER |
Total fluid used in treatment (bbls): | 255 | Max pressure during treatment (psi): | |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 95 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 160 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 10/6/2016 | Treatment End Date: | 10/6/2016 |
Treatment Summary: | PUMPED 2000 GALLONS 15% HCL AND 30 GALLONS MUSOL SOLVENT, 200 BBLS FRESH WATER |
Total fluid used in treatment (bbls): | 248 | Max pressure during treatment (psi): | |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 48 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 200 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 10/31/2014 | Treatment End Date: | 10/31/2014 |
Treatment Summary: | PUMPED 4000 GALLONS 15% HCL |
Total fluid used in treatment (bbls): | 234 | Max pressure during treatment (psi): | 2350 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 95 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 139 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Date: | 3/10/2010 |
Treatment Summary: | ACID STIMULATION 3/10/2010 PUMPED 4000 GALLONS OF 20% HCI THROUGH END OF TUBING 5719.5' AT 1 BPM AT A STARTING PRESSURE OF 2572 PSI |