Formation Treatment |
Treatment Type: | |
Treatment Date: | 12/7/2017 | Treatment End Date: | N/A |
Treatment Summary: | High casing pressure was found on FL Larson B11, the well was shut in and wellwork was completed. Replace tubing and packer, a witnessed MIT was completed on 11/16/2017.
First water injection date 10/10/1963. |
Total fluid used in treatment (bbls): | | Max pressure during treatment (psi): | |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | |
Treatment Date: | 6/26/2017 | Treatment End Date: | N/A |
Treatment Summary: | TUBING PLUG WAS SET AT 5837' ON 5/23/2017. CONVERTED TO INJECTION 10/7/1963 |
Total fluid used in treatment (bbls): | | Max pressure during treatment (psi): | |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |