| Formation Treatment |
| Treatment Type: | |
| Treatment Date: | 8/5/2025 | Treatment End Date: | N/A |
| Treatment Summary: | UIC Failure, replaced top pkr and FL tbg, found slow casing leak from 5,375'- 5,506', received ECMC exception to set packer outside normal MOU 300' requirement, chart test casing. Return to injection pending an approved Form 21.
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| Total fluid used in treatment (bbls): | | Max pressure during treatment (psi): | |
| Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
| Type Of gas: | | Number Of staged intervals: | |
| Total acid used in treatment (bbls): | | Min frac gradient (psi/ft): | |
| Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
| Fresh water used in treatment (bbls): | | Disposition method For flowback: | |
| Total proppant used (lbs): | | Green completions techniques utilized: | -- |
| Reason green techniques Not utilized: |
| Formation Treatment |
| Treatment Type: | |
| Treatment Date: | 8/14/2023 | Treatment End Date: | N/A |
| Treatment Summary: | THIS INJECTION WELL WAS SHUT IN 1/5/2022. WELLWORK TO CLEAN OUT, RAN LOCKSET PACKER, KS1X PACKER AND TUBING. RETURN WELL TO ACTIVE INJECTION PENDING AN APPROVED FORM 21.
|
| Total fluid used in treatment (bbls): | | Max pressure during treatment (psi): | |
| Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
| Type Of gas: | | Number Of staged intervals: | |
| Total acid used in treatment (bbls): | | Min frac gradient (psi/ft): | |
| Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
| Fresh water used in treatment (bbls): | | Disposition method For flowback: | |
| Total proppant used (lbs): | | Green completions techniques utilized: | -- |
| Reason green techniques Not utilized: |
| Formation Treatment |
| Treatment Type: | ACID JOB |
| Treatment Date: | 3/1/2023 | Treatment End Date: | 3/1/2023 |
| Treatment Summary: | Pumped 4000 gallons (95.2 bbl.) 15% HCL w/ additives and inhibitor and 45 bbl. fresh water.
Converted to injection 09/03/1991 |
| Total fluid used in treatment (bbls): | 140 | Max pressure during treatment (psi): | 2450 |
| Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
| Type Of gas: | | Number Of staged intervals: | |
| Total acid used in treatment (bbls): | 95 | Min frac gradient (psi/ft): | |
| Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
| Fresh water used in treatment (bbls): | 45 | Disposition method For flowback: | |
| Total proppant used (lbs): | | Green completions techniques utilized: | -- |
| Reason green techniques Not utilized: |
| Formation Treatment |
| Treatment Type: | ACID JOB |
| Treatment Date: | 1/4/2022 | Treatment End Date: | 1/4/2022 |
| Treatment Summary: | PUMPED 3000 GALLONS (71.4 BBLS) 15% HCL W/SOLVENT AND 45 BLS FRESH WATER |
| Total fluid used in treatment (bbls): | 116 | Max pressure during treatment (psi): | 2477 |
| Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
| Type Of gas: | | Number Of staged intervals: | |
| Total acid used in treatment (bbls): | 71 | Min frac gradient (psi/ft): | |
| Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
| Fresh water used in treatment (bbls): | 45 | Disposition method For flowback: | |
| Total proppant used (lbs): | | Green completions techniques utilized: | -- |
| Reason green techniques Not utilized: |
| Formation Treatment |
| Treatment Date: | 10/23/1979 |
| Treatment Summary: | ACID STIMULATION 2/20/06 PUMPED 3000 GALS 15% HCI THROUGH TUBING. |