Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 5/25/2022 | Treatment End Date: | 5/25/2022 |
Treatment Summary: | PUMPED 4000 GALLONS (95.2 BBLS) 15% HCL W/MUTUAL SOLVENT AND 35 BBLS WATER
CONVERT TO INJECTION 4/1/1967, CONVERTED BACK TO PRODUCTION 5/1/1997, CONVERTED BACK TO INJECTION 7/1/2008 |
Total fluid used in treatment (bbls): | 130 | Max pressure during treatment (psi): | 2050 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 95 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 35 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 7/21/2021 | Treatment End Date: | 7/21/2021 |
Treatment Summary: | PUMPED 2000 GALLONS (47.6 BBLS) 15% HCL W/6% CITRIC ACID AND 40 BBLS WATER
|
Total fluid used in treatment (bbls): | 87 | Max pressure during treatment (psi): | 2020 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 40 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 9/25/2020 | Treatment End Date: | 9/25/2020 |
Treatment Summary: | PUMPED 2000 GALLONS (47.6 BBLS) 15% HCL W/6% CITRIC ACID AND 1.9 BBLS SOLVENT, AND 43.0 BBLS FRESH WATER
PERFS 6416-6591 AND OPEN HOLE 6605-6660'. CONVERT TO INJECTION 4/1/1967, CONVERTED BACK TO PRODUCTION
5/1/1997, CONVERTED BACK TO INJECTION 7/1/2008. |
Total fluid used in treatment (bbls): | 92 | Max pressure during treatment (psi): | 2500 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 43 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | |
Treatment Date: | 6/20/2017 | Treatment End Date: | N/A |
Treatment Summary: | AC MCLAUGHLIN 18 WELLWORK HAS BEEN COMPLETED TO REPLACE TUBING AND PACKERS. TOP PACKER SET AT 6104.2
PERFS 6416-6591 AND OPEN HOLE 6605-6660'. CONVERT TO INJECTION 4/1/1967, CONVERTED BACK TO PRODUCTION 5/1/1997, CONVERTED BACK TO INJECTION 7/1/2008. |
Total fluid used in treatment (bbls): | | Max pressure during treatment (psi): | |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Date: | 2/12/2008 |
Treatment Summary: | OPEN HOLE 6605-6660'. CTI-RIH W/3 1/8" SLICK GUNS LOADED W 3 JSPF 120 DEGREE PHASED 23 GRAM CHARGES IN 5 RUNS PERFORATE 6565-6416 WITH TOTAL OF 381 HOLES. RIH WITH INJECTION STRING. |