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Wellbore #00 Wellbore Classification: GW Status: SI - 6/1/2020 Measured TD: 4011 ft. Vertical TD: 0 ft. Wellbore Data for Original Wellbore | Wellbore Classification: GW SI - 6/1/2020 | Wellbore Permit | | Permit #: | 770428 | Expiration Date: | 9/6/1977 | Prop Depth/Form: | | Surface Mineral Owner Same: | Not available | Mineral Owner: | FEDERAL | Surface Owner: | FEDERAL | Unit: | | Unit Number: | C-10075 | Formation And Spacing: | Code: DKTA , Formation: DAKOTA , Order: 0 , Unit Acreage: 320, Drill Unit: W2 |
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Wellbore Completed | Completion Date: | 6/29/1977 | Spud Date: | 6/10/1977 | Spud Date Is: | ACTUAL | Measured TD: | 4011 ft. | Measured PB depth: | 3976 ft. | True Vertical TD: | 0 ft. | True Vertical PB depth: | | Casing: | String Type: SURF, Hole Size: 12.25 in., Size: 8.625 in., Top: 0 ft., Depth: 252 ft., Weight: , Citings Type: HISTORICAL | Cement: | Sacks: 180, Top: 0 ft., Bottom: , Determination Method: | Casing: | String Type: 1ST, Hole Size: 7.875 in., Size: 4.5 in., Top: 0 ft., Depth: 4008 ft., Weight: , Citings Type: HISTORICAL | Cement: | Sacks: 0, Top: 0 ft., Bottom: , Determination Method: | Formation | Interval Top | Log Bottom | Cored | DSTs | FRONTIER | 3335 ft. | | | | DAKOTA | 3728 ft. | | | | MORRISON | 3852 ft. | | | |
Formation DKTA Formation Classification: GW Status: SI - 6/1/2020 Interval Top: 3804 ft. Interval Bottom: 3840 ft. Completed Information for Formation DAKOTA | 1st Production Date: | N/A | Choke Size: | 304.000 in. | Formation Name: | DAKOTA | Commingled: | | Production Method: | | Open Hole Completion: | |
| Tubing Size: | 2.375 in. | Tubing Setting Depth: | 3852 ft. | Tubing Packer Depth: | | Tubing Multiple Packer: | | Open Hole Top: | | Open Hole Bottom: | | Initial Test Data: | Test Date: | 7/2/1977 | Test Method: | FLOWING | Hours Tested: | 24 | Gas Type: | | Gas Disposal: | SOLD | |
Test Type | Measure |
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CALC_MCF_GAS | 612 | CASING_PRESS | 95 | MCF_GAS | 612 | TUBING_PRESS | 37.5 |
| Perforation Data: | Interval Top: | 3804 ft. | # Of Holes: | 25 | Interval Bottom: | 3840 ft. | Hole Size: | |
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Reported Plugged | N | |
Out Of Service Repurposed | N | |
Out Of Service | N | |
Inactive Exception | N | |
Noticed Inactive | Y | Noticed Date 01/16/2023 |
Defined Inactive (SI ) | Y | Defined Inactive 05/31/2020 |
Low Producing | Y | Production Period 11/2023 - 10/2024 |
Total Oil Produced (Barrels) | 0 |
Total Gas Produced (MCF) | 0 |
GOR | |
GOR Determination | MCFE |
Average BOE per Day | 0.000 |
Average MCFE per Day | 0.000 |
Federal Financial Assurance | i | |
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