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Wellbore #00 Wellbore Classification: OW Status: SI - 4/1/2018 Measured TD: 5450 ft. Vertical TD: 0 ft. Wellbore Data for Original Wellbore | Wellbore Classification: OW SI - 4/1/2018 | Wellbore Permit | | Permit #: | 19760522 | Expiration Date: | 10/24/1976 | Proposed Depth/Form: | 5250 ft. | Surface Mineral Owner Same: | Not available | Mineral Owner: | FEE | Surface Owner: | Not available | Unit: | | Unit Number: | | Formation And Spacing: | Code: SUSX , Formation: SUSSEX , Order: 0 , Unit Acreage: 40, Drill Unit: NWNE |
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Wellbore Completed | Completion Date: | 8/19/1976 | Spud Date: | 7/12/1976 | Spud Date Is: | ACTUAL | Measured TD: | 5450 ft. | Measured PB depth: | 5123 ft. | True Vertical TD: | 0 ft. | True Vertical PB depth: | | Log Types: | IES, FDC | Casing: | String Type: SURF, Hole Size: 12.25 in., Size: 8.625 in., Top: 0 ft., Depth: 600 ft., Weight: 24 , Citings Type: ACTUAL | Cement: | Sacks: 200, Top: 0 ft., Bottom: 600 ft., Determination Method: VISU | Casing: | String Type: 1ST, Hole Size: 7.875 in., Size: 4.5 in., Top: 0 ft., Depth: 5117 ft., Weight: 10.5 , Citings Type: ACTUAL | Cement: | Sacks: 250, Top: 4517 ft., Bottom: 5117 ft., Determination Method: CALC | Formation | Interval Top | Log Bottom | Cored | DSTs | SUSSEX | 4850 ft. | | | |
Formation SUSX Formation Classification: GW Status: SI - 4/1/2018 Interval Top: 4864 ft. Interval Bottom: 4936 ft. Completed Information for Formation SUSSEX | 1st Production Date: | 8/19/1976 | Choke Size: | 0.000 in. | Formation Name: | SUSSEX | Commingled: | | Production Method: | PUMPING | Open Hole Completion: | |
| Formation Treatment | Treatment Date: | 8/19/1976 | Treatment Summary: | 800 BBL OIL, 400 BBL H2O, 90,000# SAND |
| Tubing Size: | 2.375 in. | Tubing Setting Depth: | 4911 ft. | Tubing Packer Depth: | | Tubing Multiple Packer: | | Open Hole Top: | | Open Hole Bottom: | | Initial Test Data: | Test Date: | 8/19/1976 | Test Method: | PUMPING | Hours Tested: | 24 | Gas Type: | | Gas Disposal: | | |
Test Type | Measure |
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BBLS_OIL | 16 | CALC_GOR | 24063 | CASING_PRESS | 500 | MCF_GAS | 385 | TUBING_PRESS | 150 |
| Perforation Data: | Interval Top: | 4864 ft. | # Of Holes: | 72 | Interval Bottom: | 4936 ft. | Hole Size: | |
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Reported Plugged | Y | 09/11/2023 |
Out Of Service Repurposed | N | |
Out Of Service | N | |
Inactive Exception | N | |
Noticed Inactive | N | |
Defined Inactive (SI ) | Y | Defined Inactive 03/31/2018 |
Low Producing | N | |
Total Oil Produced (Barrels) | 0 |
Total Gas Produced (MCF) | 0 |
GOR | |
GOR Determination | |
Average BOE per Day | 0.000 |
Average MCFE per Day | 0.000 |
Federal Financial Assurance | i | |
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