| | Spike State CC30-06 18,19 - #491528 Information | Status: CL - 9/15/2025 |
| | Spill Type: | Release | Facility Name/No.: | Spike State CC30-06 18,19 / | | Facility Type: | SPILL OR RELEASE | Facility Status: | CL | | Date of Discovery: | 9/12/2025 | Date Closed: | 9/15/2025 | | Operator: | NOBLE ENERGY INC | Operator Number: | 100322 | | County: | WELD - #123 | Location: | NWNE 30 4N63W | | Doc Number: | 404354240 | Lat/Long: | 40.286514 / -104.486559 Source: ACTUAL based On LatLong | Municipality (if within municipal boundaries): | -- | | Waters of the State: | | Impacted Media: | | Related Remediation Project Number if work proceeding under an approved Form 27: | N/A | | | | Spill Description: | | On 8/25/2025, Spike State CC30-06 18,19 tank battery site investigation activities were completed. During the completion of the activities, no potential presence of impacted material(s) was observed/smelled. Final laboratory analytical results received on 9/12/2025, indicate the soil sample, BH01, BH02, & BH04, discovered at the bore holes located adjacent to the tank battery exceeded ECMC Table 915 standards for Naphthalene at 0.0041 mg/kg, 1-Methyl-Naphthalene at 0.0069 mg/kg (BH01), Benzo(a)Anthracene at 0.0121mg/kg (BH02), and Benzo(a)Anthracene at 0.0114 mg/kg (BH04). Groundwater was not encountered during decommissioning activities. All data collected will be submitted with the next quarterly Supplemental Form 27 for REM 26963, due by 12/7/2025. | | |
| | Resolution: | | Resolving Document: 404354240 | Closure Requested: 09/15/2025 | | Resolution: Work Procedeing under Form 27 |
| | | | Operator Information: | | Operator: | NOBLE ENERGY INC | | Oper. No. | 100322 | | Address: | 1099 18TH STREET SUITE 1500 DENVER CO 80202 | | Type of Facility: | SPILL OR RELEASE | | Fac. Name: | Spike State CC30-06 18,19 - | | County Name: | WELD | | qtrqtr: NWNE | section: 30 | township: 4N | range: 63W | meridian: 6 |
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