| Spill Type: | Spill | Facility Name/No.: | AC McLaughlin 64X Flowline / |
| Facility Type: | SPILL OR RELEASE | Facility Status: | CL |
| Date of Discovery: | 5/11/2024 | Date Closed: | 11/8/2024 |
| Operator: | SCOUT ENERGY MANAGEMENT LLC | Operator Number: | 10779 |
| County: | RIO BLANCO - #103 | Location: | SESE 15 2N103W |
| Doc Number: | 403787751 | Lat/Long: | 40.136319 / -108.937339 Source: ACTUAL based On LatLong |
Municipality (if within municipal boundaries): | -- |
| Waters of the State: | | Impacted Media: | |
Related Remediation Project Number if work proceeding under an approved Form 27: | N/A |
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| Spill Description: |
| On May 11, about 11:30 AM there was a flowline leak discovered on AC McLaughlin 64x after investigating a low flowline pressure alarm. Produced injection water and trace oil were release to ground. All fluids stayed on well pad location. Once it was discovered the operator immediately shut the well in and contained leak on location. All proper notifications were made, repair and clean up plans were made. |
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