| During routine inspection, the secondary containment had visual staining within the lined secondary containment. Around the dump line the secondary containment had been tore and free fluid had escaped through the tear. It is unknown how much was lost at this time due to this location has not been serviced since the transition from Encana to Utah Gas Corp but from the last gauging, there was not more that 20 bbl in the tank. The tank has obvious corrosion on the sides and possibly the bottom. The tank, piping, and secondary containment will have to be removed/replaced for soils to be inspected more. When a more accurate number for fluid lost is found, it will be presented in the Form 19 supplemental or in supplemental documents after remediation has started. A Form 27 is being drafted and will be submitted shortly for approval. The location was inspected last in June 2017, and a leak was not found during that time. |