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 Surface Location
 API# 05-123-19079
Well Classification: GW Status: PA - 10/15/2014
Well Name/No:HSR-CAMP #7-24A
(Click Well Name for Production Data)
Click Here for Transporter Gatherer Info
Operator:KERR MCGEE OIL & GAS ONSHORE LP - 47120
(Click Operator Name for Company Detail Report)
Federal Or State Lease #:
Facility Status:PAStatus Date10/15/2014
FacilityID:251276LocationID:336160
County:WELD #123Location:SENE 24 3N67W 6
Field:WATTENBERG - #90750Elevation:4787 ft.
Basin:DENVER (DJ) BASIN  
Planned Location:2222FNL  550 FELLat/Long: 40.211116 / -104.831802Lat/Long Source: Calculated From Footages
As Drilled Location:Footages Not AvailableLat/Long: 40.211180 / -104.831738Lat/Long Source: Field Measured
 Wellbore And Formation Details -- select either a wellbore Or formation to expand.
 

Wellbore #00             Wellbore Classification: GW             Status: PA - 10/15/2014             Measured TD: 7913 ft.    Vertical TD: 7481 ft.

 Wellbore Data for Original WellboreWellbore Classification: GW        PA - 10/15/2014
Wellbore PermitDIRECTIONAL
Permit #:20011261 Expiration Date:6/28/2002
Proposed Depth/Form:8300 ft.
Surface Mineral Owner Same:Yes
Mineral Owner:FEESurface Owner:Not available
Unit: Unit Number: 
Formation And Spacing:Code: JSND , Formation: J SAND , Order: 232 , Unit Acreage: 320, Drill Unit: E2
Formation And Spacing:Code: NB-CD , Formation: NIOBRARA-CODELL , Order: 0 , Unit Acreage: 80, Drill Unit: W2NE

Wellbore Completed
Completion Date:5/2/1996
Spud Date:3/30/1996Spud Date Is:ACTUAL
Measured TD:7913 ft.Measured PB depth:7867 ft.
True Vertical TD:7481 ft.True Vertical PB depth:
Log Types:DIL/SFL/GR; CBL; CDEN/GR
Casing:String Type: SURF, Hole Size: 12.25 in., Size: 8.625 in., Top: , Depth: 753 ft., Weight: 24 , Citings Type: ACTUAL
Cement:Sacks: 600, Top: 0 ft., Bottom: 753 ft., Determination Method: CALC
Casing:String Type: 1ST, Hole Size: 7.875 in., Size: 3.5 in., Top: , Depth: 7887 ft., Weight: 7.7 , Citings Type: ACTUAL
Cement:Sacks: 200, Top: 6878 ft., Bottom: 7887 ft., Determination Method: CBL
Casing:String Type: 1ST LINER, Hole Size: 3.125 in., Size: 2.375 in., Top: , Depth: 8302 ft., Weight: 4.6 , Citings Type: ACTUAL
Cement:Sacks: 14, Top: 7600 ft., Bottom: 8302 ft., Determination Method: CALC
FormationInterval TopLog BottomCoredDSTs
SUSSEX4563 ft.NN
SHANNON5487 ft.NN
NIOBRARA7423 ft.NN
FORT HAYS7680 ft.NN
CODELL7700 ft.NN
GREENHORN7758 ft.NN

Formation CODL                     Formation Classification:  GW                     Status:  CM - 5/2/1996                  Interval Top: 7706 ft.    Interval Bottom: 7714 ft.

 Completed Information for Formation CODELL
1st Production Date:5/2/1996Choke Size: 
Formation Name:CODELLCommingled:No
Production Method:
Open Hole Completion:No
Formation Treatment
Treatment Date:4/28/2005
Treatment Summary:After numerous attempts to remove a fish downhole, the tubing stuck @ 7658'. Worked the tubing for 4.5 hrs, backed off and left wash pipe and shoe in hole. Abandoned this completion.
Formation Treatment
Treatment Date:5/2/1996
Treatment Summary:
Tubing Size:Tubing Setting Depth:
Tubing Packer Depth:Tubing Multiple Packer:
Open Hole Top:Open Hole Bottom:
No Initial Test Data was found for formation CODL.
Perforation Data:
Interval Top:7706 ft.# Of Holes:41
Interval Bottom:7714 ft.Hole Size:

Formation NB-CD                   Formation Classification:  GW                   Status:  CM - 10/15/2014                Interval Top: 7490 ft.    Interval Bottom: 7711 ft.

 Completed Information for Formation NIOBRARA-CODELL
1st Production Date:5/2/1996Choke Size:1,264.000 in.
Formation Name:NIOBRARA-CODELLCommingled:
Production Method:
Open Hole Completion:
Formation Treatment
Treatment Date:5/2/1996
Treatment Summary:FRACD W/ 7500# 100 MESH 425000# 20/40 MESH 113862 GAL GELLED FLUID
Tubing Size:2.062 in.Tubing Setting Depth:7676 ft.
Tubing Packer Depth:Tubing Multiple Packer:
Open Hole Top:Open Hole Bottom:
Initial Test Data:
Test Date:6/8/1996Test Method:FLOWING
Hours Tested:24Gas Type:SHALE
Gas Disposal:SOLD
Test TypeMeasure
BBLS_H2O 0
BBLS_OIL 32
CALC_BBLS_H2O 0
CALC_BBLS_OIL 32
CALC_GOR 5719
CALC_MCF_GAS 183
CASING_PRESS 1500
GRAVITY_OIL 60
MCF_GAS 183
TUBING_PRESS 1350
Perforation Data:
Interval Top:7490 ft.# Of Holes:17
Interval Bottom:7711 ft.Hole Size:0.31 in.

Formation NBRR                     Formation Classification:  GW                     Status:  AB - 10/15/2014                Interval Top: 7436 ft.    Interval Bottom: 7492 ft.

 Completed Information for Formation NIOBRARA
1st Production Date:5/11/2005Choke Size: 
Formation Name:NIOBRARACommingled:No
Production Method:
Open Hole Completion:No
Formation Treatment
Treatment Date:5/11/2005
Treatment Summary:5/11/05- NB producing only after workover event. Codell abandoned due to fish and stuck tbg @ 7658'.
Formation Treatment
Treatment Date:5/2/1996
Treatment Summary:
Tubing Size:Tubing Setting Depth:
Tubing Packer Depth:Tubing Multiple Packer:
Open Hole Top:Open Hole Bottom:
Initial Test Data:
Test Date:1/19/2011Test Method:FLOWING
Hours Tested:24Gas Type:SHALE
Gas Disposal:SOLD
Test TypeMeasure
BBLS_H2O 0
BBLS_OIL 1
BTU_GAS 1297
CALC_BBLS_OIL 1
CALC_GOR 7000
CALC_MCF_GAS 7
CASING_PRESS 659
GRAVITY_OIL 52
MCF_GAS 7
TUBING_PRESS 701
Perforation Data:
Interval Top:7436 ft.# Of Holes:12
Interval Bottom:7492 ft.Hole Size:
Primary Well Designation:
None      i
            All DesignationsDate
Reported PluggedY10/15/2014
Out Of Service RepurposedN 
Out Of ServiceN 
Inactive ExceptionN 
Noticed InactiveN 
Defined InactiveN 
Low ProducingN 

BOE/MCFE/GOR Calculations
Production for Previous 12 Months
January 2025 - December 2025i
Total Oil Produced (Barrels)0
Total Gas Produced (MCF)0
GOR
GOR Determination 
Average BOE per Day0.000
Average MCFE per Day0.000

 Federal Financial Assurance  i 

 Tribal Well  i No