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Wellbore #00 Wellbore Classification: OW Status: PA - 5/29/2019 Measured TD: 5335 ft. Wellbore Data for Original Wellbore | Wellbore Classification: OW PA - 5/29/2019 | Wellbore Permit | DRIFTED | Permit #: | 19460650 | Expiration Date: | 11/26/1976 | Proposed Depth/Form: | 5300 ft. | Surface Mineral Owner Same: | No | Mineral Owner: | FEE | Surface Owner: | Not available | Unit: | | Unit Number: | | Formation And Spacing: | Code: SX-SN , Formation: SUSSEX-SHANNON , Order: , Unit Acreage: 80, Drill Unit: E2NE |
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Wellbore Completed | Completion Date: | 9/1/1976 | Spud Date: | 8/17/1976 | Spud Date Is: | ACTUAL | Measured TD: | 5335 ft. | Measured PB depth: | 5305 ft. | True Vertical TD: | | True Vertical PB depth: | | Log Types: | IES, FDC GR CALIPER | Casing: | String Type: SURF, Hole Size: 12.25 in., Size: 8.625 in., Top: 0 ft., Depth: 639 ft., Weight: 23 , Citings Type: ACTUAL | Cement: | Sacks: 500, Top: 0 ft., Bottom: 639 ft., Determination Method: VISU | Casing: | String Type: 1ST, Hole Size: 7.875 in., Size: 4.5 in., Top: 0 ft., Depth: 5340 ft., Weight: 11.6 , Citings Type: ACTUAL | Cement: | Sacks: 350, Top: 4268 ft., Bottom: 5340 ft., Determination Method: CALC | Formation | Interval Top | Log Bottom | Cored | DSTs | SUSSEX | 4721 ft. | | | | SHANNON | 5184 ft. | | | |
Formation SX-SN Formation Classification: GW Status: AB - 5/29/2019 Interval Top: 4626 ft. Interval Bottom: 5211 ft. Completed Information for Formation SUSSEX-SHANNON | 1st Production Date: | 9/19/1976 | Choke Size: | 0.234 in. | Formation Name: | SUSSEX-SHANNON | Commingled: | | Production Method: | FLOWING | Open Hole Completion: | |
| Formation Treatment | Treatment Date: | 9/1/1976 | Treatment Summary: | 180 BBL 10/20 2#/GAL, 57,000 GAL SUPER K, 500 GAL 7.5% ACID, 30,000# 20/40, 110,000GAL. 10/20 138,000 GAL SUPER K, 1,000 GAL 7.5% ACID, 75,000# 20/40 M, 260,000# 10/20 M |
| Tubing Size: | 2.375 in. | Tubing Setting Depth: | 4565 ft. | Tubing Packer Depth: | | Tubing Multiple Packer: | | Open Hole Top: | | Open Hole Bottom: | | Initial Test Data: | Test Date: | 9/20/1976 | Test Method: | FLOWING | Hours Tested: | 24 | Gas Type: | | Gas Disposal: | SOLD | |
Test Type | Measure |
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BBLS_H2O | 8 | BBLS_OIL | 79 | CASING_PRESS | 500 | GRAVITY_OIL | 41.8 | MCF_GAS | 202 | TUBING_PRESS | 200 |
| Perforation Data: | Interval Top: | 4626 ft. | # Of Holes: | 68 | Interval Bottom: | 5211 ft. | Hole Size: | 0.39 in. |
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Reported Plugged | Y | 05/29/2019 |
Out Of Service Repurposed | N | |
Out Of Service | N | |
Inactive Exception | N | |
Noticed Inactive | N | |
Defined Inactive | N | |
Low Producing | N | |
Total Oil Produced (Barrels) | 0 |
Total Gas Produced (MCF) | 0 |
GOR | |
GOR Determination | |
Average BOE per Day | 0.000 |
Average MCFE per Day | 0.000 |
Federal Financial Assurance | i | |
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