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COGIS - WELL SCOUT CARD

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 Surface Location
 API# 05-103-09289
Well Classification: ERIW Status: IJ - 9/1/2021
Well Name/No:GRAY #B-14A
(Click Well Name for Production Data)
Click Here for Transporter Gatherer Info
Operator:SCOUT ENERGY MANAGEMENT LLC - 10779
(Click Operator Name for Company Detail Report)
Federal Or State Lease #:
Facility Status:IJStatus Date9/1/2021
FacilityID:231618LocationID:315811
County:RIO BLANCO #103Location:SESW 18 2N102W 6
Field:RANGELY - #72370Elevation:5429 ft.
Planned Location:662FSL  2011 FWLLat/Long: 40.137595 / -108.888237Lat/Long Source: Calculated From Footages
As Drilled Location:Footages Not AvailableLat/Long: 40.137630 / -108.888130Lat/Long Source: Field Measured
 Wellbore And Formation Details -- select either a wellbore Or formation to expand.
 

Wellbore #00             Wellbore Classification: DSPW             Status: IJ - 9/1/2021             Measured TD: 6683 ft.    Vertical TD: 6680 ft.

 Wellbore Data for Original WellboreWellbore Classification: DSPW        IJ - 9/1/2021
Wellbore Permit
Permit #:870474 Expiration Date:11/7/1987
Prop Depth/Form:
Surface Mineral Owner Same:Not available
Mineral Owner:FEESurface Owner:Not available
Unit: Unit Number:D-032703-B
Formation And Spacing:Code: WEBR , Formation: WEBER , Order: 0 , Unit Acreage: 0, Drill Unit:

Wellbore Completed
Completion Date:10/29/1987
Measured TD:6683 ft.Measured PB depth:6640 ft.
True Vertical TD:6680 ft.True Vertical PB depth:
Casing:String Type: CONDUCTOR, Hole Size: , Size: 16 in., Top: 0 ft., Depth: 65 ft., Weight: , Citings Type: ACTUAL
Cement:Sacks: , Top: , Bottom: , Determination Method:
Casing:String Type: SURF, Hole Size: 12.25 in., Size: 9.625 in., Top: 0 ft., Depth: 1804 ft., Weight: 36 , Citings Type: ACTUAL
Cement:Sacks: 630, Top: 0 ft., Bottom: 1804 ft., Determination Method: VISU
Casing:String Type: 1ST, Hole Size: 8.75 in., Size: 7 in., Top: 0 ft., Depth: 6683 ft., Weight: 23&26 , Citings Type: ACTUAL
Cement:Sacks: 1610, Top: 444 ft., Bottom: 6683 ft., Determination Method: CBL
FormationInterval TopLog BottomCoredDSTs
DAKOTA3620 ft.
MORRISON3709 ft.
ENTRADA4509 ft.
NAVAJO4707 ft.
CHINLE5325 ft.
WEBER6215 ft.

Formation WEBR                     Formation Classification:  ERIW                     Status:  IJ - 9/1/2021                  Interval Top: 6232 ft.    Interval Bottom: 6592 ft.

 Completed Information for Formation WEBER
1st Production Date:3/23/1969Choke Size: 
Formation Name:WEBERCommingled:
Production Method:
Open Hole Completion:
Formation Treatment
Treatment Type:ACID JOB
Treatment Date:7/23/2021Treatment End Date:7/23/2021
Treatment Summary:UIC REPAIR WELLWORK TO CLEAN OUT, ACIDIZE AND REPLACE PACKERS. PLAN RETURN TO INJECTION, PENDING AN APPROVED MIT. PUMPED 2000 GALLONS (47.6 BBLS) 15% HCL W/6% CITRIC ACID. CONVERTED TO INJECTION MARCH 23, 1969
Total fluid used in treatment (bbls):47Max pressure during treatment (psi):1800
Total gas used in treatment (mcf):Fluid density (lbs/gal):
Type Of gas:Number Of staged intervals:
Total acid used in treatment (bbls):47Min frac gradient (psi/ft):
Recycled water used in treatment (bbls):Total flowback volume recovered (bbls):
Fresh water used in treatment (bbls):Disposition method For flowback:
Total proppant used (lbs):Green completions techniques utilized:--
Reason green techniques Not utilized: 
Formation Treatment
Treatment Type:ACID JOB
Treatment Date:10/29/2013Treatment End Date:10/29/2013
Treatment Summary:PUMPED 4000 GALLONS 15% HCL THRU END OF COILED TUBING AT 6535'
Total fluid used in treatment (bbls):170Max pressure during treatment (psi):1500
Total gas used in treatment (mcf):Fluid density (lbs/gal):
Type Of gas:Number Of staged intervals:
Total acid used in treatment (bbls):95Min frac gradient (psi/ft):
Recycled water used in treatment (bbls):Total flowback volume recovered (bbls):
Fresh water used in treatment (bbls):75Disposition method For flowback:
Total proppant used (lbs):Green completions techniques utilized:--
Reason green techniques Not utilized: 
Formation Treatment
Treatment Date:10/6/2010
Treatment Summary:ACID STIMULATION 10/06/2010 PUMPED 4000 GALLONS OF 20% HCL THROUGH COILED TUBING AT 6600'. STARTING PRESSURE OF 1500 PSI.
Formation Treatment
Treatment Date:8/17/2009
Treatment Summary:ACID STIMULATION 8/17/09 PUMPED 2000 GALS 20% HCI & 10,500 GALS CLO2 IN FOUR STAGES THROUGH TUBING @ 6534'. AVERAGE 3.6 BPM @ 2191 PSI.
Tubing Size:2.875 in.Tubing Setting Depth:6100 ft.
Tubing Packer Depth:6000 ft.Tubing Multiple Packer:
Open Hole Top:Open Hole Bottom:
No Initial Test Data was found for formation WEBR.
Perforation Data:
Interval Top:6232 ft.# Of Holes:176
Interval Bottom:6592 ft.Hole Size:0.5 in.
Primary Well Designation:
None      i
            All DesignationsDate
Reported PluggedN 
Out Of Service RepurposedN 
Out Of ServiceN 
Inactive ExceptionN 
Noticed InactiveN 
Defined InactiveN 
Low ProducingN 

BOE/MCFE/GOR Calculations
Production for Previous 12 Months
June 2023 - May 2024i
Total Oil Produced (Barrels)0
Total Gas Produced (MCF)148279
GOR
GOR DeterminationMCFE
Average BOE per Day70.171
Average MCFE per Day406.983

 Federal Financial Assurance  i Y

 Tribal Well  i No