| Formation Treatment |
| Treatment Type: | ACID JOB |
| Treatment Date: | 9/23/2024 | Treatment End Date: | 9/23/2024 |
| Treatment Summary: | UIC repair, POOH w/ both pkrs, CO fr/ 5903'-6750', tst'd csg - failed, isolated leak at 4354'-4386', est inj rate of 0.19 BPM @ 2700 psi, spot acid to help breakdown leak, new inj rate of 2.1 BPM @ 1700 psi, mixed 28 sxs (8 bbls) 13.4# Premium G cmt down tbg, spot cmt plug, set pkr and sqz a total of 2.9 bbls into leak, let cmt dry, DO cmt and tst csg - good tst, RIH w/ inj pkrs and FL tbg, RDMO. Return to injection pending an approved Form 21.
1487 bbls of fresh water used, recycled 1450 bbls, 260 bbls brine lost downhole for a total fluid used of 1747 bbls.
Well converted to injection 08/22/2006 |
| Total fluid used in treatment (bbls): | 1747 | Max pressure during treatment (psi): | 1700 |
| Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
| Type Of gas: | | Number Of staged intervals: | |
| Total acid used in treatment (bbls): | 6 | Min frac gradient (psi/ft): | |
| Recycled water used in treatment (bbls): | 1450 | Total flowback volume recovered (bbls): | |
| Fresh water used in treatment (bbls): | 1487 | Disposition method For flowback: | |
| Total proppant used (lbs): | | Green completions techniques utilized: | -- |
| Reason green techniques Not utilized: |
| Formation Treatment |
| Treatment Type: | ACID JOB |
| Treatment Date: | 5/16/2024 | Treatment End Date: | 5/16/2024 |
| Treatment Summary: | PUMPED 2000 GALLONS (47.6 BBLS) 15% HCL W/SOLVENT AND 150 BBLS FRESH WATER. |
| Total fluid used in treatment (bbls): | 287 | Max pressure during treatment (psi): | 200 |
| Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
| Type Of gas: | | Number Of staged intervals: | |
| Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
| Recycled water used in treatment (bbls): | 90 | Total flowback volume recovered (bbls): | |
| Fresh water used in treatment (bbls): | 150 | Disposition method For flowback: | |
| Total proppant used (lbs): | | Green completions techniques utilized: | -- |
| Reason green techniques Not utilized: |
| Formation Treatment |
| Treatment Type: | ACID JOB |
| Treatment Date: | 4/12/2024 | Treatment End Date: | 4/12/2024 |
| Treatment Summary: | PUMPED 2000 GALLONS (47.6 BBLS) 15% HCL W/SOLVENT AND 35 BBLS FRESH WATER. |
| Total fluid used in treatment (bbls): | 82 | Max pressure during treatment (psi): | 2500 |
| Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
| Type Of gas: | | Number Of staged intervals: | |
| Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
| Recycled water used in treatment (bbls): | 0 | Total flowback volume recovered (bbls): | |
| Fresh water used in treatment (bbls): | 35 | Disposition method For flowback: | |
| Total proppant used (lbs): | | Green completions techniques utilized: | -- |
| Reason green techniques Not utilized: |
| Formation Treatment |
| Treatment Type: | ACID JOB |
| Treatment Date: | 2/17/2021 | Treatment End Date: | 2/17/2021 |
| Treatment Summary: | PUMPED 2000 GALLONS (47.6 BBLS) 15% HCL W/6% CITRIC ACID AND MUTUAL SOLVENT, 47 BBLS WATER |
| Total fluid used in treatment (bbls): | 95 | Max pressure during treatment (psi): | 2300 |
| Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
| Type Of gas: | | Number Of staged intervals: | |
| Total acid used in treatment (bbls): | 48 | Min frac gradient (psi/ft): | |
| Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
| Fresh water used in treatment (bbls): | 47 | Disposition method For flowback: | |
| Total proppant used (lbs): | | Green completions techniques utilized: | -- |
| Reason green techniques Not utilized: |
| Formation Treatment |
| Treatment Type: | ACID JOB |
| Treatment Date: | 9/14/2019 | Treatment End Date: | 9/14/2019 |
| Treatment Summary: | PUMPED 2000 GALLONS (47.6 BBLS) 15% HCL WITH 6% CITRIC ACID, 80 BBLS OF WATER. |
| Total fluid used in treatment (bbls): | 127 | Max pressure during treatment (psi): | 2200 |
| Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
| Type Of gas: | | Number Of staged intervals: | |
| Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
| Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
| Fresh water used in treatment (bbls): | 80 | Disposition method For flowback: | |
| Total proppant used (lbs): | | Green completions techniques utilized: | -- |
| Reason green techniques Not utilized: |
| Formation Treatment |
| Treatment Type: | ACID JOB |
| Treatment Date: | 3/20/2015 | Treatment End Date: | 3/20/2015 |
| Treatment Summary: | PUMPED 4000 GALLONS 15% HCL |
| Total fluid used in treatment (bbls): | 178 | Max pressure during treatment (psi): | 1950 |
| Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
| Type Of gas: | | Number Of staged intervals: | |
| Total acid used in treatment (bbls): | 95 | Min frac gradient (psi/ft): | |
| Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
| Fresh water used in treatment (bbls): | 83 | Disposition method For flowback: | |
| Total proppant used (lbs): | | Green completions techniques utilized: | -- |
| Reason green techniques Not utilized: |