Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 11/20/2021 | Treatment End Date: | 11/20/2021 |
Treatment Summary: | PUMPED 2000 GALLONS (47.6 bbls) 15% HCL w/6% CITRIC ACID AND MUTUAL SOLVENT AND 40 BBLS WATER.
|
Total fluid used in treatment (bbls): | 87 | Max pressure during treatment (psi): | 2400 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 40 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 3/18/2021 | Treatment End Date: | 3/18/2021 |
Treatment Summary: | PUMPED 2000 GALLONS (47.6 bbls) 15% HCL w/6% CITRIC ACID AND MUTUAL SOLVENT AND 33 BBLS WATER.
CONVERTED TO INJECTION DECEMBER 1996.
Corrections to perferations reported on previous Form 5A |
Total fluid used in treatment (bbls): | 82 | Max pressure during treatment (psi): | 1800 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 33 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 10/17/2018 | Treatment End Date: | 10/18/2018 |
Treatment Summary: | PUMPED 4000 GALLONS 15 HCL WITH 50 BBLS WATER. CEMENT SQUEEZE CASING LEAK. CONVERTED TO INJECTION DECEMBER 1996. |
Total fluid used in treatment (bbls): | 145 | Max pressure during treatment (psi): | 1800 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 95 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 50 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Date: | 8/7/2009 |
Treatment Summary: | ACID STIMULATION 8/6/09 PUMPED 2000 GALS HEATED 20% HCI & 10,500 GALS CHLORINE DIOXIDE IN FOUR STAGES THROUGH TUBING AT 6246. AVERAGE 4.2 BPM & 2216 PSI. |