Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 7/24/2024 | Treatment End Date: | 7/24/2024 |
Treatment Summary: | Pumped 2000 gallons (47.6 bbls) 15% HCL w/solvent and 35 bbls Fresh Water |
Total fluid used in treatment (bbls): | 82 | Max pressure during treatment (psi): | 2500 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | 0 | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 35 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | |
Treatment Date: | 12/7/2022 | Treatment End Date: | N/A |
Treatment Summary: | Well work to replace 7" PS1 pkr and FL inj tbg, Space out, Set pkr, Land well, ND BOPE, NU inj tree, Perform passing pre-MIT chart on annulus and passing tbg test. Return to injection pending an approved Form 21. |
Total fluid used in treatment (bbls): | | Max pressure during treatment (psi): | |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 5/24/2022 | Treatment End Date: | 5/24/2022 |
Treatment Summary: | Pumped 4000 gallons (95.2 BBLS) 15% HCL w/Solvent and 35 BBLS Fresh water
Converted to injection 09/25/73 |
Total fluid used in treatment (bbls): | 130 | Max pressure during treatment (psi): | 2450 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 95 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 35 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Date: | 4/12/2011 |
Treatment Summary: | ACID STIMULATION WITH 3000 GALLONS 20% HCL THROUGH END OF COILED TUBING @ 6380' AT STARTING PRESSURE OF 600 PSI |