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Wellbore #00 Wellbore Classification: ERIW Status: SI - 4/1/2020 Measured TD: 5687 ft.| Wellbore Data for Original Wellbore | Wellbore Classification: ERIW SI - 4/1/2020 | | Wellbore Permit | | | Permit #: | 19540000 | Expiration Date: | 5/17/1955 | | Proposed Depth/Form: | 5725 ft. | | Surface Mineral Owner Same: | Not available | | Mineral Owner: | FEE | Surface Owner: | Not available | | Unit: | ADENA J SAND UNIT | Unit Number: | | | Formation And Spacing: | Code: JSND , Formation: J SAND , Order: , Unit Acreage: , Drill Unit: |
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| Wellbore Completed | | Completion Date: | 7/2/1954 | | Spud Date: | 6/23/1954 | Spud Date Is: | ACTUAL | | Measured TD: | 5687 ft. | Measured PB depth: | | | True Vertical TD: | | True Vertical PB depth: | | | Casing: | String Type: SURF, Hole Size: , Size: 8.625 in., Top: , Depth: 117 ft., Weight: 24 , Citings Type: ACTUAL | | Cement: | Sacks: 100, Top: , Bottom: , Determination Method: | | Casing: | String Type: 1ST, Hole Size: , Size: 5.5 in., Top: , Depth: 5683 ft., Weight: 14 , Citings Type: ACTUAL | | Cement: | Sacks: 150, Top: , Bottom: , Determination Method: | | Formation | Interval Top | Log Bottom | Cored | DSTs | | NIOBRARA | 4739 ft. | | | | | FORT HAYS | 5087 ft. | | | | | CARLILE | 5134 ft. | | | | | GREENHORN | 5196 ft. | | | | | BENTONITE | 5443 ft. | | | | | D SAND | 5538 ft. | | | | | J SAND | 5607 ft. | | | |
Formation JSND Formation Classification: ERIW Status: SI - 4/1/2020 Interval Top: 5608 ft. Interval Bottom: 5666 ft.| Completed Information for Formation J SAND | | 1st Production Date: | N/A | Choke Size: | | | Formation Name: | J SAND | Commingled: | No | | Production Method: | | | Open Hole Completion: | |
| | Formation Treatment | | Treatment Type: | ACID JOB | | Treatment Date: | 10/15/2014 | Treatment End Date: | 10/15/2014 | | Treatment Summary: | This Adena J Sand Unit injection well was not taking fluid. Most recent MIT - 6/25/13. The well was cleaned out to below original
perfs. Perforated 5608-5624 (6 spf) and 5634-5666 (6 spf). Re-set the injection packer at 5570 ft. The well was then acidized with 59.5 bbls 15% HCL. The acid job was followed by injection water and the well was returned to injection status. | | Total fluid used in treatment (bbls): | 120 | Max pressure during treatment (psi): | 1467 | | Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | 8.38 | | Type Of gas: | | Number Of staged intervals: | 1 | | Total acid used in treatment (bbls): | 60 | Min frac gradient (psi/ft): | 0.43 | | Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | 120 | | Fresh water used in treatment (bbls): | | Disposition method For flowback: | RECYCLE | | Total proppant used (lbs): | | Green completions techniques utilized: | Yes | | Reason green techniques Not utilized: |
| | Tubing Size: | | Tubing Setting Depth: | | | Tubing Packer Depth: | | Tubing Multiple Packer: | | | Open Hole Top: | | Open Hole Bottom: | | | Initial Test Data: | | Test Date: | N/A | Test Method: | | | Hours Tested: | | Gas Type: | | | Gas Disposal: | | |
| Test Type | Measure |
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| BBLS_OIL | 1035 | | CALC_GOR | 500 | | GRAVITY_OIL | 43 | | TUBING_PRESS | 130 |
| | Perforation Data: | | Interval Top: | 5608 ft. | # Of Holes: | 288 | | Interval Bottom: | 5666 ft. | Hole Size: | |
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| Reported Plugged | N | |
| Out Of Service Repurposed | N | |
| Out Of Service | N | |
| Inactive Exception | N | |
| Noticed Inactive | N | |
| Defined Inactive (UIC) | Y | Last Use 03/31/2020 |
| Low Producing | N | |
| Total Oil Produced (Barrels) | 0 |
| Total Gas Produced (MCF) | 0 |
| GOR | |
| GOR Determination | |
| Average BOE per Day | 0.000 |
| Average MCFE per Day | 0.000 |
| Federal Financial Assurance | i | |
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