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Wellbore #00 Wellbore Classification: OW Status: IJ - 8/1/2023 Measured TD: 5002 ft. Vertical TD: 4937 ft. Wellbore Data for Original Wellbore | Wellbore Classification: OW IJ - 8/1/2023 | Wellbore Permit | DIRECTIONAL | Permit #: | 19920946 | Expiration Date: | 12/13/1992 | Proposed Depth/Form: | 5066 ft. | Surface Mineral Owner Same: | Yes | Mineral Owner: | FEE | Surface Owner: | FEE | Unit: | MUDDY SANDSTONE | Unit Number: | | Formation And Spacing: | Code: MDDYJ , Formation: MUDDY J , Order: 84-2 , Unit Acreage: 0, Drill Unit: |
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Wellbore Completed | Completion Date: | 10/2/1992 | Spud Date: | 8/19/1992 | Spud Date Is: | ACTUAL | Measured TD: | 5002 ft. | Measured PB depth: | 4934 ft. | True Vertical TD: | 4937 ft. | True Vertical PB depth: | 4870 ft. | Log Types: | DIL, GR, DENSITY NEUTRON | Casing: | String Type: SURF, Hole Size: 12.25 in., Size: 9.625 in., Top: 0 ft., Depth: 492 ft., Weight: 36 , Citings Type: ACTUAL | Cement: | Sacks: 330, Top: 0 ft., Bottom: , Determination Method: | Casing: | String Type: 1ST, Hole Size: 8.75 in., Size: 5.5 in., Top: , Depth: 4998 ft., Weight: 15.5 , Citings Type: ACTUAL | Cement: | Sacks: 250, Top: 3868 ft., Bottom: , Determination Method: | Formation | Interval Top | Log Bottom | Cored | DSTs | NIOBRARA | 4000 ft. | | | | FORT HAYS | 4325 ft. | | | | CODELL | 4349 ft. | | | | BENTONITE | 4623 ft. | | | | MUDDY J | 4866 ft. | | | |
Formation MDDYJ Formation Classification: GW Status: IJ - 8/1/2023 Interval Top: 4866 ft. Interval Bottom: 4924 ft. Completed Information for Formation MUDDY J | 1st Production Date: | 5/2/1995 | Choke Size: | | Formation Name: | MUDDY J | Commingled: | | Production Method: | INJECTION | Open Hole Completion: | |
| Formation Treatment | Treatment Date: | 10/2/1992 | Treatment Summary: | BROKE DOWN PERF W/1000 GAL 3% HCL, FRAC W/155,000# 16/30 SAND IN CROSSLINKED WATER BASE GEL |
| Tubing Size: | 2.875 in. | Tubing Setting Depth: | 4817 ft. | Tubing Packer Depth: | | Tubing Multiple Packer: | | Open Hole Top: | | Open Hole Bottom: | | Initial Test Data: | Test Date: | 10/18/1992 | Test Method: | BEAM PUMP | Hours Tested: | | Gas Type: | | Gas Disposal: | | |
Test Type | Measure |
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CALC_BBLS_H2O | 253.3 | CALC_BBLS_OIL | 149.9 | CASING_PRESS | 14 | GRAVITY_OIL | 36 |
| Perforation Data: | Interval Top: | 4866 ft. | # Of Holes: | 59 | Interval Bottom: | 4924 ft. | Hole Size: | 0.4 in. |
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Reported Plugged | N | |
Out Of Service Repurposed | N | |
Out Of Service | N | |
Inactive Exception | N | |
Noticed Inactive | N | |
Defined Inactive (UIC) | Y | Defined Inactive 12/31/2023 |
Low Producing | N | |
Total Oil Produced (Barrels) | 0 |
Total Gas Produced (MCF) | 0 |
GOR | |
GOR Determination | |
Average BOE per Day | 0.000 |
Average MCFE per Day | 0.000 |
Federal Financial Assurance | i | |
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