|
|
| |
|
|
|
|
Wellbore #00 Wellbore Classification: OW Status: SI - 1/1/2022 Measured TD: 4890 ft. Vertical TD: 0 ft.| Wellbore Data for Original Wellbore | Wellbore Classification: OW SI - 1/1/2022 | | Wellbore Permit | | | Permit #: | 19670207 | Expiration Date: | 5/25/1968 | | Proposed Depth/Form: | 4800 ft. | | Surface Mineral Owner Same: | Not available | | Mineral Owner: | FEE | Surface Owner: | Not available | | Unit: | | Unit Number: | | | Formation And Spacing: | Code: MSSP , Formation: MISSISSIPPIAN , Order: 0 , Unit Acreage: 80, Drill Unit: E2NW |
| | |
| Wellbore Completed | | Completion Date: | 7/22/1967 | | Spud Date: | 6/4/1967 | Spud Date Is: | ACTUAL | | Measured TD: | 4890 ft. | Measured PB depth: | 0 ft. | | True Vertical TD: | 0 ft. | True Vertical PB depth: | | | Casing: | String Type: SURF, Hole Size: 12.25 in., Size: 8.625 in., Top: 0 ft., Depth: 194 ft., Weight: 24 , Citings Type: ACTUAL | | Cement: | Sacks: 175, Top: 0 ft., Bottom: 194 ft., Determination Method: VISU | | Casing: | String Type: 1ST, Hole Size: 7.875 in., Size: 5.5 in., Top: 0 ft., Depth: 4889 ft., Weight: 15.5 , Citings Type: ACTUAL | | Cement: | Sacks: 100, Top: 4260 ft., Bottom: 4889 ft., Determination Method: CALC | | Formation | Interval Top | Log Bottom | Cored | DSTs | | VIRGIL | 3236 ft. | | | | | LANSING | 3590 ft. | | | | | MARMATON | 3974 ft. | | | | | CHEROKEE K | 4112 ft. | | | | | MORROW | 4386 ft. | | | | | MISSISSIPPIAN | 4582 ft. | | | | | OSAGE | 4848 ft. | | | |
Formation MSSP Formation Classification: GW Status: SI - 1/1/2022 Interval Top: 4783 ft. Interval Bottom: 4866 ft.| Completed Information for Formation MISSISSIPPIAN | | 1st Production Date: | 7/22/1967 | Choke Size: | 0.000 in. | | Formation Name: | MISSISSIPPIAN | Commingled: | | | Production Method: | | | Open Hole Completion: | |
| | Tubing Size: | 2.875 in. | Tubing Setting Depth: | 4758 ft. | | Tubing Packer Depth: | 4765 ft. | Tubing Multiple Packer: | | | Open Hole Top: | | Open Hole Bottom: | | | Initial Test Data: | | Test Date: | 7/22/1967 | Test Method: | | | Hours Tested: | 24 | Gas Type: | | | Gas Disposal: | | |
| Test Type | Measure |
|---|
| BBLS_OIL | 150 | | CALC_BBLS_OIL | 150 | | CASING_PRESS | 30 | | GRAVITY_OIL | 38 |
| | Perforation Data: | | Interval Top: | 4783 ft. | # Of Holes: | | | Interval Bottom: | 4866 ft. | Hole Size: | |
|
|
|
|
|
|
|
| Reported Plugged | Y | 03/31/2024 |
| Out Of Service Repurposed | N | |
| Out Of Service | Y | Plugging Due Date 12/31/2028 |
| Inactive Exception | N | |
| Noticed Inactive | N | |
| Defined Inactive (SI ) | Y | Defined Inactive 12/31/2021 |
| Low Producing | N | |
| Total Oil Produced (Barrels) | 0 |
| Total Gas Produced (MCF) | 0 |
| GOR | |
| GOR Determination | |
| Average BOE per Day | 0.000 |
| Average MCFE per Day | 0.000 |
| Federal Financial Assurance | i | |
|
|